ITAC Assessment: UF0443
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ITAC Assessment: UF0443
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Assessment Year 2011
Principal Product Milk, Juice, Tea, Water
NAICS 311511: Fluid Milk Manufacturing
SIC 2026: Fluid Milk
Sales Range $50
M
to 100
M
# of Employees 114
Plant Area 135,000
ft2
Annual Production 36,000,000
Tgal
Production Hrs. Annual 8,760
hrs
Location (State) Florida

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $1,100,107 15,474,296
kWh
Electricity Demand $370,867 61,602
kW-mo/yr
Natural Gas $47,488 25,311
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $266,278 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $60,249

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Electricity Demand Savings Natural Gas Savings
01 2.7124: Make a practice of turning off lights when not needed $1,607 - $1,607
22,636
kWh
- -
02 2.7142: Utilize higher efficiency lamps and/or ballasts $38,731 $42,492 $34,375
484,149
kWh
$4,356
-
kW-mo/yr
-
03 2.4226: Use / purchase optimum sized compressor $9,454 $38,200 $9,454
99,520
kWh
- -
04 2.7229: Air condition only space necessary $4,722 $550 $4,722
66,501
kWh
- -
05 2.7261: Install timers and/or thermostats $562 $75 $562
5,918
kWh
- -
06 2.7224: Reduce space conditioning during non-working hours $19,349 $2,235 $19,349
203,670
kWh
- -
07 2.6231: Utilize controls to operate equipment only when needed $106,353 $25,300 $106,353
1,497,934
kWh
- -
08 2.2135: Repair and eliminate steam leaks $156 $370 - - $156
-
MMBtu
09 2.4146: Use adjustable frequency drive or multiple speed motors on existing system $80,522 $8,600 $80,522
847,600
kWh
- -
10 2.4131: Size electric motors for peak operating efficiency $4,822 $670 $4,822
67,914
kWh
- -
TOTAL RECOMMENDED $266,278 $118,492 $261,766
3,295,842
kWh
$4,356
-
kW-mo/yr
$156
-
MMBtu
TOTAL IMPLEMENTED $60,249 $44,802 $55,893
716,373
kWh
$4,356
-
kW-mo/yr
-
Yearly Savings* Imp'd Cost* Electricity Usage Savings Electricity Demand Savings Natural Gas Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs