| Assessment Year | 2008 |
|---|---|
| Principal Product | soy milk |
| NAICS | 311514: Dry, Condensed, and Evaporated Dairy Product Manufacturing |
| SIC | 2026: Fluid Milk |
| Sales Range | $1 M to 5M |
| # of Employees | 101 |
| Plant Area |
185,000
ft2
|
| Annual Production | 17,200,000
pieces
|
| Production Hrs. Annual | 7,488
hrs
|
| Location (State) | Florida |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | |
|---|---|---|---|---|
| Electricity Usage | $576,888 | 8,022,466 |
kWh
|
$0.072 |
| Natural Gas | $502,803 | 52,600 |
MMBtu
|
$9.56 |
| TOTAL YEARLY COSTS | - | |||
| RECOMMENDED SAVINGS* | $183,593 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
| IMPLEMENTED SAVINGS* | $83,774 | |||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
|---|---|---|---|---|---|---|
| 01 | 2.7135: Install occupancy sensors | $207 | $79 |
$207
3,564
kWh
|
- | |
| 02 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $24,683 | $42,414 |
$24,683
365,602
kWh
|
- | |
| 03 | 2.4224: Upgrade controls on compressors | $12,505 | $731 |
$12,505
215,612
kWh
|
- | |
| 04 | 2.1113: Reduce combustion air flow to optimum | $1,855 | $795 | - |
$1,855
-
MMBtu
|
|
| 05 | 2.2135: Repair and eliminate steam leaks | $17,781 | $615 | - |
$17,781
-
MMBtu
|
|
| 06 | 2.4151: Develop a repair/replace policy | $2,521 | - |
$2,521
34,521
kWh
|
- | |
| 07 | 2.7245: Use direct air supply to exhaust hoods | $2,081 | $534 |
$2,081
38,812
kWh
|
- | |
| 08 | 2.6232: Install set-back timers | $15,103 | $4,916 |
$15,103
262,543
kWh
|
- | |
| 09 | 2.7225: Close outdoor air dampers during warm-up / cool-down periods | $1,822 | $10,480 |
$1,822
31,410
kWh
|
- | |
| 10 | 2.2441: Preheat boiler makeup water with waste process heat | $95,676 | $20,000 | - |
$95,676
-
MMBtu
|
|
| 11 | 2.1131: Repair faulty insulation in furnaces, boilers, etc | $9,359 | $4,246 | - |
$9,359
-
MMBtu
|
|
| TOTAL RECOMMENDED | $183,593 | $84,810 |
$58,922
952,064
kWh
|
$124,671
-
MMBtu
|
||
| TOTAL IMPLEMENTED | $83,774 | $63,402 |
$56,634
909,688
kWh
|
$27,140
-
MMBtu
|
||
| Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | |||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs