ITAC Assessment: GT0274
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ITAC Assessment: GT0274
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Assessment Year 1985
Principal Product MENS'& BOYS' UNDERWEAR
NAICS
n/a
SIC 2254: Knit Underwear and Nightwear Mills
Sales Range $10
M
to 50
M
# of Employees 669
Plant Area
n/a
Annual Production 12,400,000
pieces
Production Hrs. Annual 1,960
hrs
Location (State) Georgia

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $249,525 4,271,981
kWh
Natural Gas $62,587 12,923
MMBtu
Fuel Oil #6 $14,162 2,584
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $61,334 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $61,334

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Natural Gas Savings Fuel Oil #6 Savings
01 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves $18,590 $250 $18,590
317,995
kWh
- -
02 2.7142: Utilize higher efficiency lamps and/or ballasts $6,568 $560 $6,568
112,544
kWh
- -
03 2.1224: Replace boiler $11,945 $32,000 - $9,769
-
MMBtu
$2,176
-
MMBtu
04 2.4221: Install compressor air intakes in coolest locations $550 $600 $550
9,379
kWh
- -
05 2.7261: Install timers and/or thermostats $8,866 - - $7,252
-
MMBtu
$1,614
-
MMBtu
06 2.7447: Install vinyl strip / high speed / air curtain doors $1,882 $2,280 - $1,542
-
MMBtu
$340
-
MMBtu
07 2.4133: Use most efficient type of electric motors $993 $894 $993
16,999
kWh
- -
08 2.3191: Use demand controller or load shedder $11,940 $15,000 $11,940
-
kWh
- -
TOTAL RECOMMENDED $61,334 $51,584 $38,641
456,917
kWh
$18,563
-
MMBtu
$4,130
-
MMBtu
TOTAL IMPLEMENTED $61,334 $51,584 $38,641
456,917
kWh
$18,563
-
MMBtu
$4,130
-
MMBtu
Yearly Savings* Imp'd Cost* Electricity Usage Savings Natural Gas Savings Fuel Oil #6 Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs