ITAC Assessment: CO0015
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ITAC Assessment: CO0015
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Assessment Year 1984
Principal Product WELDING EQUIPMENT
NAICS
n/a
SIC 3549: Metalworking Machinery, Not Elsewhere Classified
Sales Range $1
M
to 5
M
# of Employees 180
Plant Area
n/a
Annual Production 55
pieces
Production Hrs. Annual 4,368
hrs
Location (State) Colorado

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $52,460 895,369
kWh
Natural Gas $23,444 5,682
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $14,847 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $6,049

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Natural Gas Savings Administrative Changes Savings
01 2.7142: Utilize higher efficiency lamps and/or ballasts $963 $908 $963
17,585
kWh
- -
02 2.1233: Analyze flue gas for proper air/fuel ratio $300 $300 - $300
-
MMBtu
-
03 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves $290 $50 $290
5,275
kWh
- -
04 2.7492: Use proper thickness of insulation on building envelope $694 $1,127 - $694
-
MMBtu
-
05 2.7261: Install timers and/or thermostats $5,808 $4,000 - $5,808
-
MMBtu
-
06 2.7447: Install vinyl strip / high speed / air curtain doors $791 $230 - $791
-
MMBtu
-
07 2.7316: Centralize control of exhaust fans to ensure their shutdown, or establish program to ensure manual shutdown $1,240 $103 $256
4,689
kWh
$984
-
MMBtu
-
08 2.7121: Utilize daylight whenever possible in lieu of artificial light $293 $120 $293
4,982
kWh
- -
09 2.3512: De-energize excess transformer capacity $220 $100 $220
4,103
kWh
- -
10 2.3131: Reschedule plant operations or reduce load to avoid peaks $2,676 $5,000 $3,636
-
kWh
- $(-960.0)
11 2.4235: Remove or close off unneeded compressed air lines $335 $250 $335
6,155
kWh
- -
12 2.7252: Utilize an evaporative air pre-cooler or other heat exchanger in ac system $1,237 $3,000 - $1,237
-
MMBtu
-
TOTAL RECOMMENDED $14,847 $15,188 $5,993
42,789
kWh
$9,814
-
MMBtu
$(-960.0)
TOTAL IMPLEMENTED $6,049 $7,865 $5,224
29,015
kWh
$1,785
-
MMBtu
$(-960.0)
Yearly Savings* Imp'd Cost* Electricity Usage Savings Natural Gas Savings Administrative Changes Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs