Assessment Year | 1989 |
---|---|
Principal Product | PLYWOOD |
NAICS |
n/a
|
SIC | 2435: Hardwood Veneer and Plywood |
Sales Range | $1 M to 5M |
# of Employees | 375 |
Plant Area |
n/a
|
Annual Production | 120
thousand feet
|
Production Hrs. Annual | 6,916
hrs
|
Location (State) | Washington |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $528,822 | 19,317,996 |
kWh
|
$0.027 |
Wood | $786,880 | 1,205,023 |
MMBtu
|
$0.65 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $324,177 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $21,686 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Wood Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|
01 | 2.1233: Analyze flue gas for proper air/fuel ratio | $9,642 | - | - |
$9,642
-
MMBtu
|
- | |
02 | 2.6232: Install set-back timers | $5,010 | - |
$3,383
172,626
kWh
|
- | $1,627 | |
03 | 2.6218: Turn off equipment when not in use | $2,409 | - |
$2,409
123,095
kWh
|
- | - | |
04 | 2.3131: Reschedule plant operations or reduce load to avoid peaks | $17,258 | $370 |
$17,258
-
kWh
|
- | - | |
05 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $9,867 | $2,499 |
$1,431
53,048
kWh
|
- | $8,436 | |
06 | 2.4221: Install compressor air intakes in coolest locations | $1,848 | $500 |
$1,848
68,581
kWh
|
- | - | |
07 | 2.2441: Preheat boiler makeup water with waste process heat | $4,272 | $2,814 | - |
$4,272
-
MMBtu
|
- | |
08 | 2.4133: Use most efficient type of electric motors | $704 | $576 |
$704
26,084
kWh
|
- | - | |
09 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $2,552 | $3,000 |
$2,552
94,666
kWh
|
- | - | |
10 | 2.3212: Optimize plant power factor | $2,056 | $3,300 |
$2,056
-
kWh
|
- | - | |
11 | 3.7214: Reduce or eliminate waste | $268,559 | $1,000,000 |
$(-31,097.0)
(-916,471)
kWh
|
$10,741
-
MMBtu
|
$288,915 | |
TOTAL RECOMMENDED | $324,177 | $1,013,059 |
$544
(-378,371)
kWh
|
$24,655
-
MMBtu
|
$298,978 | ||
TOTAL IMPLEMENTED | $21,686 | $5,999 |
$11,623
512,016
kWh
|
- | $10,063 | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Wood Savings | Administrative Changes Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs