Assessment Year | 2016 |
---|---|
Principal Product | Corrugated boxes, shipping supplies, bottled water, pressed paper produc |
NAICS | 322211: Corrugated and Solid Fiber Box Manufacturing |
SIC | 2653: Corrugated and Solid Fiber Boxes |
Sales Range | $10 M to 50M |
# of Employees | 100 |
Plant Area |
307,000
ft2
|
Annual Production | 13,300,000
units
|
Production Hrs. Annual | 8,760
hrs
|
Location (State) | Texas |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | ||
---|---|---|---|---|---|
Electricity Usage | $132,209 | 3,672,480 |
kWh
|
$0.036 | |
Electricity Demand | $149,826 | 12,583 |
kW-mo/yr
|
$11.91 | |
Electricity Fees | $16,679 | - |
|
- | |
Natural Gas | $129,692 | 28,646 |
MMBtu
|
$4.53 | |
Waste Disposal Costs | |||||
Water Usage | $89,773 | 18,462 |
Tgal
|
$4.86 | |
Water Disposal | $46,620 | 18,462 |
Tgal
|
$2.53 | |
TOTAL YEARLY COSTS | $564,799 | ||||
RECOMMENDED SAVINGS* | $102,576 |
See individual recommendations below
*Non-energy impacts included in savings.
|
|||
IMPLEMENTED SAVINGS* | $94,200 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Electricity Fees Savings | Natural Gas Savings | Water Disposal Savings |
---|---|---|---|---|---|---|---|---|---|
01 | 3.4116: Meter recycled water (to reduce sewer charges) | $40,741 | $19,000 | - | - | - | - |
$40,741
-
Tgal
|
|
02 | 2.8123: Pay utility bills on time | $21,826 | - | - | - | $21,826 | - | - | |
03 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $7,211 | - |
$7,211
225,307
kWh
|
- | - | - | - | |
04 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $4,792 | $250 |
$4,792
133,117
kWh
|
- | - | - | - | |
05 | 2.4322: Use or replace with energy efficient substitutes | $3,584 | $1,350 |
$3,584
99,558
kWh
|
- | - | - | - | |
06 | 2.4221: Install compressor air intakes in coolest locations | $645 | $1,405 |
$645
17,920
kWh
|
- | - | - | - | |
07 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $7,445 | $11,700 |
$7,445
206,801
kWh
|
- | - | - | - | |
08 | 2.1131: Repair faulty insulation in furnaces, boilers, etc | $5,953 | $4,600 | - | - | - |
$5,953
-
MMBtu
|
- | |
09 | 2.7241: Install outside air damper / economizer on hvac unit | $1,934 | $2,720 |
$1,934
53,718
kWh
|
- | - | - | - | |
10 | 2.6232: Install set-back timers | $1,250 | $790 |
$281
7,801
kWh
|
- | - |
$969
-
MMBtu
|
- | |
11 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $6,334 | $21,372 |
$4,119
114,409
kWh
|
$2,215
-
kW-mo/yr
|
- | - | - | |
12 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $861 | $4,032 |
$389
10,816
kWh
|
$472
-
kW-mo/yr
|
- | - | - | |
TOTAL RECOMMENDED | $102,576 | $67,219 |
$30,400
869,447
kWh
|
$2,687
-
kW-mo/yr
|
$21,826 |
$6,922
-
MMBtu
|
$40,741
-
Tgal
|
||
TOTAL IMPLEMENTED | $94,200 | $65,619 |
$22,024
636,772
kWh
|
$2,687
-
kW-mo/yr
|
$21,826 |
$6,922
-
MMBtu
|
$40,741
-
Tgal
|
||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Electricity Fees Savings | Natural Gas Savings | Water Disposal Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs