Assessment Year | 2013 |
---|---|
Principal Product | Carbinated beverages |
NAICS | 312111: Soft Drink Manufacturing |
SIC | 2086: Bottled and Canned Soft Drinks and Carbonated Waters |
Sales Range | $5 M to 10M |
# of Employees | 125 |
Plant Area |
500,000
ft2
|
Annual Production | 7,000,000
units
|
Production Hrs. Annual | 2,600
hrs
|
Location (State) | Texas |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $275,164 | 3,633,887 |
kWh
|
$0.076 |
Natural Gas | $37,106 | 8,691 |
MMBtu
|
$4.27 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $50,143 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $27,331 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
---|---|---|---|---|---|---|
01 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $3,788 | $27,500 |
$3,788
49,838
kWh
|
- | |
02 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $2,073 | $600 |
$2,073
27,276
kWh
|
- | |
03 | 2.2437: Recover waste heat from equipment | $1,413 | $1,378 | - |
$1,413
-
MMBtu
|
|
04 | 2.4231: Reduce the pressure of compressed air to the minimum required | $1,327 | - |
$1,327
17,456
kWh
|
- | |
05 | 2.4221: Install compressor air intakes in coolest locations | $360 | $1,575 |
$360
4,731
kWh
|
- | |
06 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $673 | $8,267 |
$673
8,850
kWh
|
- | |
07 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $1,885 | $7,053 |
$1,885
24,480
kWh
|
- | |
08 | 2.1224: Replace boiler | $6,063 | $60,000 | - |
$6,063
-
MMBtu
|
|
09 | 2.7232: Replace existing hvac unit with high efficiency model | $5,770 | $21,632 |
$5,770
75,923
kWh
|
- | |
10 | 2.1231: Establish burner maintenance schedule for boilers | $1,310 | $4,958 |
$1,310
16,374
kWh
|
- | |
11 | 2.7241: Install outside air damper / economizer on hvac unit | $3,220 | $3,650 |
$3,220
42,360
kWh
|
- | |
12 | 2.6232: Install set-back timers | $2,987 | $2,259 |
$1,884
24,789
kWh
|
$1,103
-
MMBtu
|
|
13 | 2.4322: Use or replace with energy efficient substitutes | $4,448 | - |
$4,448
58,522
kWh
|
- | |
14 | 2.4131: Size electric motors for peak operating efficiency | $14,826 | $25,000 |
$14,826
195,075
kWh
|
- | |
TOTAL RECOMMENDED | $50,143 | $163,872 |
$41,564
545,674
kWh
|
$8,579
-
MMBtu
|
||
TOTAL IMPLEMENTED | $27,331 | $34,392 |
$26,228
344,223
kWh
|
$1,103
-
MMBtu
|
||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs