| Assessment Year | 2010 |
|---|---|
| Principal Product | Aerospace parts |
| NAICS | 336411: Aircraft Manufacturing |
| SIC | 3721: Aircraft |
| Sales Range | $10 M to 50M |
| # of Employees | 116 |
| Plant Area |
100,000
ft2
|
| Annual Production | 103,000
pieces
|
| Production Hrs. Annual | 6,240
hrs
|
| Location (State) | Oklahoma |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | |
|---|---|---|---|---|
| Electricity Usage | $152,163 | 3,119,209 |
kWh
|
$0.049 |
| Electricity Demand | $57,917 | 7,796 |
kW-mo/yr
|
$7.43 |
| Natural Gas | $11,091 | 1,022 |
MMBtu
|
$10.85 |
| TOTAL YEARLY COSTS | - | |||
| RECOMMENDED SAVINGS* | $41,326 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
| IMPLEMENTED SAVINGS* | $25,999 | |||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Fees Savings | Natural Gas Savings |
|---|---|---|---|---|---|---|---|
| 01 | 2.7492: Use proper thickness of insulation on building envelope | $6,511 | $78,169 |
$386
7,906
kWh
|
- |
$6,125
-
MMBtu
|
|
| 02 | 2.7232: Replace existing hvac unit with high efficiency model | $4,599 | $34,948 |
$4,599
94,232
kWh
|
- | - | |
| 03 | 2.7211: Clean and maintain refrigerant condensers and towers | $9,699 | $3,000 |
$9,699
198,744
kWh
|
- | - | |
| 04 | 2.7232: Replace existing hvac unit with high efficiency model | $995 | $2,625 | - | - |
$995
-
MMBtu
|
|
| 05 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $3,205 | $660 |
$3,205
72,976
kWh
|
- | - | |
| 06 | 2.4221: Install compressor air intakes in coolest locations | $523 | $516 |
$523
10,726
kWh
|
- | - | |
| 07 | 2.2437: Recover waste heat from equipment | $3,015 | $2,017 | - | - |
$3,015
-
MMBtu
|
|
| 08 | 2.7135: Install occupancy sensors | $547 | $1,658 |
$547
11,212
kWh
|
- | - | |
| 09 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $299 | $201 |
$299
6,132
kWh
|
- | - | |
| 10 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $7,069 | $14,336 |
$7,069
144,853
kWh
|
- | - | |
| 11 | 2.3212: Optimize plant power factor | $669 | $9,307 | - | $669 | - | |
| 12 | 2.2691: Shut off cooling if cold outside air will cool process | $4,196 | $21,075 |
$4,196
85,978
kWh
|
- | - | |
| TOTAL RECOMMENDED | $41,326 | $168,512 |
$30,523
632,759
kWh
|
$669 |
$10,135
-
MMBtu
|
||
| TOTAL IMPLEMENTED | $25,999 | $139,817 |
$18,880
386,860
kWh
|
- |
$7,120
-
MMBtu
|
||
| Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Fees Savings | Natural Gas Savings | |||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs