Assessment Year | 1984 |
---|---|
Principal Product | VACUUM TANKS |
NAICS |
n/a
|
SIC | 3713: Truck and Bus Bodies |
Sales Range | $10 M to 50M |
# of Employees | 75 |
Plant Area |
n/a
|
Annual Production | 650
pieces
|
Production Hrs. Annual | 2,730
hrs
|
Location (State) | Oklahoma |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $21,035 | 266,999 |
kWh
|
$0.079 |
Natural Gas | $19,190 | 3,806 |
MMBtu
|
$5.04 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $6,009 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $5,025 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
---|---|---|---|---|---|---|
01 | 2.7261: Install timers and/or thermostats | $4,492 | $1,100 | - |
$4,492
-
MMBtu
|
|
02 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $58 | $48 |
$58
1,465
kWh
|
- | |
03 | 2.7444: Close holes and openings in building such as broken windows | $141 | $336 |
$141
3,224
kWh
|
- | |
04 | 2.7229: Air condition only space necessary | $334 | - |
$334
7,620
kWh
|
- | |
05 | 2.3512: De-energize excess transformer capacity | $984 | - |
$984
-
kWh
|
- | |
TOTAL RECOMMENDED | $6,009 | $1,484 |
$1,517
12,309
kWh
|
$4,492
-
MMBtu
|
||
TOTAL IMPLEMENTED | $5,025 | $1,484 |
$533
12,309
kWh
|
$4,492
-
MMBtu
|
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs