| Assessment Year | 1984 |
|---|---|
| Principal Product | OIL RESEARCH VEHICLES |
| NAICS |
n/a
|
| SIC | 3531: Construction Machinery and Equipment |
| Sales Range | $5 M to 10M |
| # of Employees | 50 |
| Plant Area |
n/a
|
| Annual Production | 50
pieces
|
| Production Hrs. Annual | 2,500
hrs
|
| Location (State) | Oklahoma |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | |
|---|---|---|---|---|
| Electricity Usage | $14,738 | 446,659 |
kWh
|
$0.033 |
| Natural Gas | $24,932 | 3,495 |
MMBtu
|
$7.13 |
| TOTAL YEARLY COSTS | - | |||
| RECOMMENDED SAVINGS* | $6,609 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
| IMPLEMENTED SAVINGS* | $2,246 | |||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
|---|---|---|---|---|---|---|
| 01 | 2.5123: Reduce fluid flow rates | $4,300 | $3,000 | - |
$4,300
-
MMBtu
|
|
| 02 | 2.7261: Install timers and/or thermostats | $1,080 | $900 | - |
$1,080
-
MMBtu
|
|
| 03 | 2.6212: Turn off equipment during breaks, reduce operating time | $294 | $200 | - |
$294
-
MMBtu
|
|
| 04 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $676 | $306 |
$676
13,775
kWh
|
- | |
| 05 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $34 | $27 |
$34
1,172
kWh
|
- | |
| 06 | 2.6232: Install set-back timers | $162 | $110 |
$162
5,569
kWh
|
- | |
| 07 | 2.7111: Reduce illumination to minimum necessary levels | $63 | $10 |
$63
1,172
kWh
|
- | |
| TOTAL RECOMMENDED | $6,609 | $4,553 |
$935
21,688
kWh
|
$5,674
-
MMBtu
|
||
| TOTAL IMPLEMENTED | $2,246 | $1,543 |
$872
20,516
kWh
|
$1,374
-
MMBtu
|
||
| Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | |||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs