Assessment Year | 1982 |
---|---|
Principal Product | WINCHES, POWER TAKE-OFF |
NAICS |
n/a
|
SIC | 3531: Construction Machinery and Equipment |
Sales Range | $1 M to 5M |
# of Employees | 275 |
Plant Area |
n/a
|
Annual Production | 5,000
pieces
|
Production Hrs. Annual | 4,000
hrs
|
Location (State) | Oklahoma |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $145,825 | 4,027,550 |
kWh
|
$0.036 |
Natural Gas | $25,000 | 8,300 |
MMBtu
|
$3.01 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $16,699 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | - |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
---|---|---|---|---|---|---|
01 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $7,801 | $180 |
$7,801
283,411
kWh
|
- | |
02 | 2.4221: Install compressor air intakes in coolest locations | $187 | $330 |
$187
6,741
kWh
|
- | |
03 | 2.2532: Use only amount of air necessary to prevent explosion hazard | $199 | $17 |
$34
1,172
kWh
|
$165
-
MMBtu
|
|
04 | 2.2532: Use only amount of air necessary to prevent explosion hazard | $7,642 | $80 |
$1,042
37,808
kWh
|
$6,600
-
MMBtu
|
|
05 | 2.7261: Install timers and/or thermostats | $275 | $790 | - |
$275
-
MMBtu
|
|
06 | 2.5123: Reduce fluid flow rates | $595 | - |
$100
3,810
kWh
|
$495
-
MMBtu
|
|
TOTAL RECOMMENDED | $16,699 | $1,397 |
$9,164
332,942
kWh
|
$7,535
-
MMBtu
|
||
TOTAL IMPLEMENTED | - | - | - | - | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs