Assessment Year | 2014 |
---|---|
Principal Product | Tobacco |
NAICS | 312230: Tobacco Manufacturing |
SIC | 2141: Tobacco Stemming and Redrying |
Sales Range | $10 M to 50M |
# of Employees | 46 |
Plant Area |
120,000
ft2
|
Annual Production | 22,000,000
lb
|
Production Hrs. Annual | 3,600
hrs
|
Location (State) | North Carolina |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $198,956 | 3,247,200 |
kWh
|
$0.061 |
Electricity Demand | $46,043 | 10,848 |
kW-mo/yr
|
$4.24 |
Natural Gas | $261,061 | 51,686 |
MMBtu
|
$5.05 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $47,023 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $37,113 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Personnel Changes Savings | Ancillary Material Cost Savings |
---|---|---|---|---|---|---|---|---|---|
01 | 2.4226: Use / purchase optimum sized compressor | $15,335 | $3,500 |
$15,335
250,174
kWh
|
- | - | - | - | |
02 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $13,235 | $880 |
$13,338
217,584
kWh
|
$2,977
-
kW-mo/yr
|
- | $(-2,600.0) | $(-480.0) | |
03 | 2.2437: Recover waste heat from equipment | $924 | $1,150 | - | - |
$924
-
MMBtu
|
- | - | |
04 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $4,931 | $25,335 |
$4,060
66,226
kWh
|
$372
-
kW-mo/yr
|
- | - | $499 | |
05 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $1,747 | $8,956 |
$1,385
22,601
kWh
|
$362
-
kW-mo/yr
|
- | - | - | |
06 | 2.7124: Make a practice of turning off lights when not needed | $3,222 | $100 |
$3,222
52,566
kWh
|
- | - | - | - | |
07 | 2.7135: Install occupancy sensors | $847 | $900 |
$847
13,817
kWh
|
- | - | - | - | |
08 | 2.2123: Insulate feedwater tank | $1,294 | $387 | - | - |
$1,294
-
MMBtu
|
- | - | |
09 | 2.2136: Install / repair insulation on steam lines | $505 | $766 | - | - |
$505
-
MMBtu
|
- | - | |
10 | 2.5123: Reduce fluid flow rates | $3,623 | $3,000 |
$2,963
48,341
kWh
|
$660
-
kW-mo/yr
|
- | - | - | |
11 | 2.4151: Develop a repair/replace policy | $1,360 | $4,256 |
$1,112
18,133
kWh
|
$248
-
kW-mo/yr
|
- | - | - | |
TOTAL RECOMMENDED | $47,023 | $49,230 |
$42,262
689,442
kWh
|
$4,619
-
kW-mo/yr
|
$2,723
-
MMBtu
|
$(-2,600.0) | $19 | ||
TOTAL IMPLEMENTED | $37,113 | $43,693 |
$35,230
574,718
kWh
|
$3,959
-
kW-mo/yr
|
$505
-
MMBtu
|
$(-2,600.0) | $19 | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Personnel Changes Savings | Ancillary Material Cost Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs