Assessment Year | 1984 |
---|---|
Principal Product | AIR CONDITIONING EQUIPMENT |
NAICS |
n/a
|
SIC | 3564: Industrial and Commercial Fans and Blowers and Air Purification Equipment |
Sales Range | $10 M to 50M |
# of Employees | 200 |
Plant Area |
n/a
|
Annual Production | 100,000
pieces
|
Production Hrs. Annual | 2,082
hrs
|
Location (State) | Kansas |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $106,293 | 1,558,910 |
kWh
|
$0.068 |
Natural Gas | $38,123 | 9,011 |
MMBtu
|
$4.23 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $23,327 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $9,801 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|
01 | 2.7314: Reduce ventilation air | $11,229 | - |
$3,137
46,014
kWh
|
$8,092
-
MMBtu
|
- | |
02 | 2.3191: Use demand controller or load shedder | $3,395 | $4,000 |
$3,395
-
kWh
|
- | - | |
03 | 2.4312: Improve lubrication practices | $1,597 | - |
$3,097
45,428
kWh
|
- | $(-1,500.0) | |
04 | 2.1123: Install automatic stack damper | $2,157 | $1,900 | - |
$2,157
-
MMBtu
|
- | |
05 | 2.7211: Clean and maintain refrigerant condensers and towers | $1,578 | - |
$2,078
30,481
kWh
|
- | $(-500.0) | |
07 | 2.7447: Install vinyl strip / high speed / air curtain doors | $1,279 | $39 |
$40
586
kWh
|
$1,239
-
MMBtu
|
- | |
08 | 2.1233: Analyze flue gas for proper air/fuel ratio | $160 | - | - |
$660
-
MMBtu
|
$(-500.0) | |
09 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $1,039 | $500 |
$1,039
15,240
kWh
|
- | - | |
10 | 2.2437: Recover waste heat from equipment | $753 | $400 |
$440
6,448
kWh
|
$313
-
MMBtu
|
- | |
11 | 2.4221: Install compressor air intakes in coolest locations | $140 | $200 |
$140
2,052
kWh
|
- | - | |
TOTAL RECOMMENDED | $23,327 | $7,039 |
$13,366
146,249
kWh
|
$12,461
-
MMBtu
|
$(-2,500.0) | ||
TOTAL IMPLEMENTED | $9,801 | $4,939 |
$10,089
98,183
kWh
|
$2,212
-
MMBtu
|
$(-2,500.0) | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs