Assessment Year | 2008 |
---|---|
Principal Product | High Voltage Electrical Switches |
NAICS | 335313: Switchgear and Switchboard Apparatus Manufacturing |
SIC | 3613: Switchgear and Switchboard Apparatus |
Sales Range | $50 M to 100M |
# of Employees | 340 |
Plant Area |
175,000
ft2
|
Annual Production | 17,000
pieces
|
Production Hrs. Annual | 4,500
hrs
|
Location (State) | Georgia |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $159,033 | 3,334,800 |
kWh
|
$0.048 |
Electricity Demand | $123,636 | 8,076 |
kW-mo/yr
|
$15.31 |
Electricity Fees | $15,627 | - |
|
- |
Natural Gas | $105,974 | 10,675 |
MMBtu
|
$9.93 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $90,381 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $64,976 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|---|
01 | 2.6218: Turn off equipment when not in use | $11,537 | $2,000 | - | - |
$11,537
-
MMBtu
|
- | |
02 | 2.6218: Turn off equipment when not in use | $9,290 | $2,000 |
$9,290
184,875
kWh
|
- | - | - | |
03 | 2.7261: Install timers and/or thermostats | $8,620 | $3,000 | - | - |
$8,620
-
MMBtu
|
- | |
04 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $11,097 | $4,500 |
$16,097
320,089
kWh
|
- | - | $(-5,000.0) | |
05 | 2.4231: Reduce the pressure of compressed air to the minimum required | $2,723 | - |
$1,875
37,299
kWh
|
$848
-
kW-mo/yr
|
- | - | |
06 | 2.7444: Close holes and openings in building such as broken windows | $8,400 | $15,000 | - | - |
$8,400
-
MMBtu
|
- | |
07 | 2.7447: Install vinyl strip / high speed / air curtain doors | $8,385 | $13,000 | - | - |
$8,385
-
MMBtu
|
- | |
08 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $30,329 | $80,207 |
$16,098
320,303
kWh
|
$14,231
-
kW-mo/yr
|
- | - | |
TOTAL RECOMMENDED | $90,381 | $119,707 |
$43,360
862,566
kWh
|
$15,079
-
kW-mo/yr
|
$36,942
-
MMBtu
|
$(-5,000.0) | ||
TOTAL IMPLEMENTED | $64,976 | $88,707 |
$43,360
862,566
kWh
|
$15,079
-
kW-mo/yr
|
$11,537
-
MMBtu
|
$(-5,000.0) | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Administrative Changes Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs