ITAC Assessment: GT0423
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ITAC Assessment: GT0423
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Assessment Year 1990
Principal Product EXTRUDED FIBERS
NAICS
n/a
SIC 2299: Textile goods, Not Elsewhere Classified
Sales Range $10
M
to 50
M
# of Employees 200
Plant Area
n/a
Annual Production 15,000,000
lb
Production Hrs. Annual 8,400
hrs
Location (State) South Carolina

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $347,510 7,880,129
kWh
Natural Gas $59,954 13,151
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $45,317 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $24,353

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Natural Gas Savings
01 2.7111: Reduce illumination to minimum necessary levels $5,280 - $5,280
121,630
kWh
-
02 2.7142: Utilize higher efficiency lamps and/or ballasts $9,135 $10,029 $9,135
210,434
kWh
-
03 2.4133: Use most efficient type of electric motors $668 $500 $668
15,533
kWh
-
04 2.4312: Improve lubrication practices $2,000 - $2,000
46,014
kWh
-
05 2.4231: Reduce the pressure of compressed air to the minimum required $1,600 $2,000 $1,600
36,049
kWh
-
06 2.4239: Eliminate or reduce compressed air usage $5,500 $500 $5,500
126,905
kWh
-
07 2.6231: Utilize controls to operate equipment only when needed $2,200 $1,600 $2,200
50,117
kWh
-
08 2.1221: Replace obsolete burners with more efficient ones $3,250 $7,000 - $3,250
-
MMBtu
09 2.2614: Use cooling tower or economizer to replace chiller cooling $15,684 $11,000 $15,684
361,372
kWh
-
TOTAL RECOMMENDED $45,317 $32,629 $42,067
968,054
kWh
$3,250
-
MMBtu
TOTAL IMPLEMENTED $24,353 $21,629 $21,103
485,052
kWh
$3,250
-
MMBtu
Yearly Savings* Imp'd Cost* Electricity Usage Savings Natural Gas Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs