Assessment Year | 1995 |
---|---|
Principal Product | Steel Pipe Couplings |
NAICS |
n/a
|
SIC | 3498: Fabricated Pipe and Pipe Fittings |
Sales Range | $50 M to 100M |
# of Employees | 100 |
Plant Area |
130,000
ft2
|
Annual Production | 24,700,000
lb
|
Production Hrs. Annual | 7,509
hrs
|
Location (State) | Arkansas |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $356,023 | 6,283,118 |
kWh
|
$0.057 |
Natural Gas | $29,284 | 7,578 |
MMBtu
|
$3.86 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $33,784 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $32,816 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Water Disposal Savings | Water Consumption Savings |
---|---|---|---|---|---|---|---|---|
01 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $997 | $380 |
$997
14,947
kWh
|
- | - | - | |
02 | 2.7111: Reduce illumination to minimum necessary levels | $14,786 | $900 |
$14,786
296,600
kWh
|
- | - | - | |
03 | 2.4111: Utilize energy-efficient belts and other improved mechanisms | $1,829 | - |
$1,829
40,152
kWh
|
- | - | - | |
04 | 2.1233: Analyze flue gas for proper air/fuel ratio | $490 | $1,000 | - |
$490
-
MMBtu
|
- | - | |
05 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $3,615 | $300 |
$3,615
73,271
kWh
|
- | - | - | |
06 | 2.4221: Install compressor air intakes in coolest locations | $1,364 | $400 |
$1,364
27,550
kWh
|
- | - | - | |
07 | 2.4133: Use most efficient type of electric motors | $8,172 | $16,900 |
$8,172
141,852
kWh
|
- | - | - | |
08 | 2.4239: Eliminate or reduce compressed air usage | $968 | $400 |
$968
19,637
kWh
|
- | - | - | |
09 | 2.2113: Repair or replace steam traps | $420 | $100 | - |
$420
-
MMBtu
|
- | - | |
10 | 3.4151: Minimize water usage | $1,143 | $100 | - | - |
$587
-
Tgal
|
$556
-
Tgal
|
|
TOTAL RECOMMENDED | $33,784 | $20,480 |
$31,731
614,009
kWh
|
$910
-
MMBtu
|
$587
-
Tgal
|
$556
-
Tgal
|
||
TOTAL IMPLEMENTED | $32,816 | $20,080 |
$30,763
594,372
kWh
|
$910
-
MMBtu
|
$587
-
Tgal
|
$556
-
Tgal
|
||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | Water Disposal Savings | Water Consumption Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs