Assessment Year | 1988 |
---|---|
Principal Product | STAMPINGS AND WASHERS |
NAICS |
n/a
|
SIC | 3452: Bolts, Nuts, Screws, Rivets, and Washers |
Sales Range | $10 M to 50M |
# of Employees | 240 |
Plant Area |
n/a
|
Annual Production | 28,000,000
lb
|
Production Hrs. Annual | 4,250
hrs
|
Location (State) | Wisconsin |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $192,261 | 3,749,121 |
kWh
|
$0.051 |
Natural Gas | $88,998 | 22,279 |
MMBtu
|
$3.99 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $13,128 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $5,706 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|
01 | 2.2437: Recover waste heat from equipment | $4,758 | $3,500 | - |
$4,758
-
MMBtu
|
- | |
02 | 2.1233: Analyze flue gas for proper air/fuel ratio | $1,808 | $500 | - |
$1,908
-
MMBtu
|
$(-100.0) | |
03 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $1,157 | $454 |
$1,157
22,567
kWh
|
- | - | |
04 | 2.4221: Install compressor air intakes in coolest locations | $2,548 | $2,500 |
$2,548
49,824
kWh
|
- | - | |
05 | 2.3131: Reschedule plant operations or reduce load to avoid peaks | $1,507 | - |
$2,707
-
kWh
|
- | $(-1,200.0) | |
06 | 2.1311: Replace electrically-operated equipment with fossil fuel equipment | $1,350 | $2,300 |
$2,021
39,566
kWh
|
$(-671.0)
-
MMBtu
|
- | |
TOTAL RECOMMENDED | $13,128 | $9,254 |
$8,433
111,957
kWh
|
$5,995
-
MMBtu
|
$(-1,300.0) | ||
TOTAL IMPLEMENTED | $5,706 | $5,300 |
$4,569
89,390
kWh
|
$1,237
-
MMBtu
|
$(-100.0) | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs