Assessment Year | 2007 |
---|---|
Principal Product | bottled water |
NAICS | 312112: Bottled Water Manufacturing |
SIC | 2086: Bottled and Canned Soft Drinks and Carbonated Waters |
Sales Range | $100 M to 500M |
# of Employees | 330 |
Plant Area |
425,000
ft2
|
Annual Production | 1,030,000,000
pieces
|
Production Hrs. Annual | 8,736
hrs
|
Location (State) | Florida |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $3,962,005 | 45,302,051 |
kWh
|
$0.087 |
Electricity Demand | $348,787 | 177,655 |
kW-mo/yr
|
$1.96 |
Natural Gas | $142,529 | 130,310 |
MMBtu
|
$1.09 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $5,057,012 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $272,457 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|---|
01 | 2.7141: Lower light fixtures in high ceiling areas | $1,441 | $253 |
$1,399
16,074
kWh
|
$42
-
kW-mo/yr
|
- | - | |
02 | 2.7121: Utilize daylight whenever possible in lieu of artificial light | $372 | $289 |
$372
4,284
kWh
|
- | - | - | |
03 | 2.6232: Install set-back timers | $6,690 | $625 |
$6,690
76,894
kWh
|
- | - | - | |
04 | 2.5195: Change product design to reduce energy requirements | $6,004 | $399 |
$6,004
63,204
kWh
|
- | - | - | |
05 | 2.2135: Repair and eliminate steam leaks | $17,857 | $619 | - | - |
$17,857
-
MMBtu
|
- | |
06 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $17,557 | $714 |
$17,557
184,808
kWh
|
- | - | - | |
07 | 2.4231: Reduce the pressure of compressed air to the minimum required | $229,959 | - |
$229,959
2,420,621
kWh
|
- | - | - | |
08 | 2.2442: Preheat combustion air with waste heat | $6,754 | $22,000 | - | - |
$6,754
-
MMBtu
|
- | |
09 | 2.2515: Use optimum thickness insulation | $7,084 | $1,380 | - | - |
$7,084
-
MMBtu
|
- | |
10 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $18,733 | $6,479 |
$18,733
197,608
kWh
|
- | - | - | |
11 | 4.631: Install an uninteruptable power supply | $4,744,561 | $5,831 | - | - | - | $4,744,561 | |
TOTAL RECOMMENDED | $5,057,012 | $38,589 |
$280,714
2,963,493
kWh
|
$42
-
kW-mo/yr
|
$31,695
-
MMBtu
|
$4,744,561 | ||
TOTAL IMPLEMENTED | $272,457 | $2,713 |
$247,516
2,605,429
kWh
|
- |
$24,941
-
MMBtu
|
- | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Administrative Changes Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs