Assessment Year | 1993 |
---|---|
Principal Product | weatherstripping, moldings, weatherseals |
NAICS |
n/a
|
SIC | 3429: Hardware, Not Elsewhere Classified |
Sales Range | $10 M to 50M |
# of Employees | 320 |
Plant Area |
192,000
ft2
|
Annual Production | 0
units
|
Production Hrs. Annual | 6,000
hrs
|
Location (State) | Ohio |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $331,616 | 6,519,930 |
kWh
|
$0.051 |
Natural Gas | $10,630 | 2,628 |
MMBtu
|
$4.04 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $47,774 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $12,718 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Other Energy Savings |
---|---|---|---|---|---|---|---|
01 | 2.3131: Reschedule plant operations or reduce load to avoid peaks | $16,277 | - |
$16,277
-
kWh
|
- | - | |
02 | 2.5123: Reduce fluid flow rates | $7,396 | $5,000 |
$(-1,410.0)
(-29,894)
kWh
|
- |
$8,806
-
MMBtu
|
|
03 | 2.2437: Recover waste heat from equipment | $12,240 | $40,000 | - |
$12,240
-
MMBtu
|
- | |
04 | 2.7111: Reduce illumination to minimum necessary levels | $156 | $200 |
$334
15,533
kWh
|
$(-178.0)
-
MMBtu
|
- | |
05 | 2.3131: Reschedule plant operations or reduce load to avoid peaks | $6,539 | - |
$6,539
63,013
kWh
|
- | - | |
06 | 2.4224: Upgrade controls on compressors | $5,166 | $800 |
$6,665
155,041
kWh
|
$(-1,499.0)
-
MMBtu
|
- | |
TOTAL RECOMMENDED | $47,774 | $46,000 |
$28,405
203,693
kWh
|
$10,563
-
MMBtu
|
$8,806
-
MMBtu
|
||
TOTAL IMPLEMENTED | $12,718 | $6,000 |
$5,589
140,680
kWh
|
$(-1,677.0)
-
MMBtu
|
$8,806
-
MMBtu
|
||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | Other Energy Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs