| Assessment Year | 2019 |
|---|---|
| Principal Product | Moist and Dry Snuff |
| NAICS | 312230: Tobacco Manufacturing |
| SIC | 2131: Chewing and Smoking Tobacco and Snuff |
| Sales Range | $100 M to 500M |
| # of Employees | 153 |
| Plant Area |
843,581
ft2
|
| Annual Production | 35,765,716
units
|
| Production Hrs. Annual | 4,160
hrs
|
| Location (State) | Tennessee |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | ||
|---|---|---|---|---|---|
| Electricity Usage | $859,271 | 14,547,840 |
kWh
|
$0.059 | |
| Electricity Demand | $342,844 | 37,335 |
kW-mo/yr
|
$9.18 | |
| Natural Gas | $298,525 | 40,116 |
MMBtu
|
$7.44 | |
| Waste Disposal Costs | |||||
| Water Usage | $93,750 | 7,809 |
Tgal
|
$12.01 | |
| Water Disposal | $38,620 | 7,809 |
Tgal
|
$4.95 | |
| Solid Waste (non-haz) | $37,500 | 1,500,000 |
lb
|
$0.025 | |
| TOTAL YEARLY COSTS | $1,670,510 | ||||
| RECOMMENDED SAVINGS* | $78,039 |
See individual recommendations below
*Non-energy impacts included in savings.
|
|||
| IMPLEMENTED SAVINGS* | $55,623 | ||||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Solid Waste (non-haz) Savings |
|---|---|---|---|---|---|---|---|---|
| 01 | 3.6192: Use a less expensive method of waste removal | $37,500 | - | - | - | - |
$37,500
-
lb
|
|
| 02 | 2.1233: Analyze flue gas for proper air/fuel ratio | $13,000 | $6,000 | - | - |
$13,000
-
MMBtu
|
- | |
| 03 | 2.4111: Utilize energy-efficient belts and other improved mechanisms | $8,935 | $39,040 |
$8,935
151,190
kWh
|
- | - | - | |
| 04 | 2.1243: Use heat from boiler blowdown to preheat boiler feed water | $6,630 | $30,000 | - | - |
$6,630
-
MMBtu
|
- | |
| 05 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $6,238 | $3,200 |
$5,187
87,770
kWh
|
$1,051
-
kW-mo/yr
|
- | - | |
| 06 | 2.2422: Use waste heat from hot flue gases to generate steam | $2,786 | $10,000 | - | - |
$2,786
-
MMBtu
|
- | |
| 07 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $2,661 | $1,618 |
$2,661
44,492
kWh
|
- | - | - | |
| 08 | 2.7261: Install timers and/or thermostats | $289 | $20 |
$289
4,892
kWh
|
- | - | - | |
| TOTAL RECOMMENDED | $78,039 | $89,878 |
$17,072
288,344
kWh
|
$1,051
-
kW-mo/yr
|
$22,416
-
MMBtu
|
$37,500
-
lb
|
||
| TOTAL IMPLEMENTED | $55,623 | $43,878 |
$17,072
288,344
kWh
|
$1,051
-
kW-mo/yr
|
- |
$37,500
-
lb
|
||
| Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Solid Waste (non-haz) Savings | |||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs