Assessment Year | 1992 |
---|---|
Principal Product | RAYON AND COATED CLOTH |
NAICS |
n/a
|
SIC | 2823: Cellulosic Manmade Fibers |
Sales Range | $50 M to 100M |
# of Employees | 1,425 |
Plant Area |
n/a
|
Annual Production | 24,000,000
lb
|
Production Hrs. Annual | 8,736
hrs
|
Location (State) | Tennessee |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $51,875 | 681,125 |
kWh
|
$0.076 |
Natural Gas | $71,145 | 12,606 |
MMBtu
|
$5.64 |
Coal | $4,811,511 | 4,000,000 |
MMBtu
|
$1.20 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $336,170 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $336,170 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Coal Savings |
---|---|---|---|---|---|---|
01 | 2.2113: Repair or replace steam traps | $157,734 | $15,225 | - |
$157,734
-
MMBtu
|
|
02 | 2.2136: Install / repair insulation on steam lines | $94,476 | $22,010 | - |
$94,476
-
MMBtu
|
|
03 | 2.4111: Utilize energy-efficient belts and other improved mechanisms | $24,383 | $7,272 | - |
$24,383
-
MMBtu
|
|
04 | 2.2135: Repair and eliminate steam leaks | $11,943 | $2,965 | - |
$11,943
-
MMBtu
|
|
05 | 2.2511: Insulate bare equipment | $3,501 | $2,366 | - |
$3,501
-
MMBtu
|
|
06 | 2.4221: Install compressor air intakes in coolest locations | $2,509 | $1,410 | - |
$2,509
-
MMBtu
|
|
07 | 2.4312: Improve lubrication practices | $1,749 | - | - |
$1,749
-
MMBtu
|
|
08 | 2.8114: Change rate schedules or other changes in utility service | $39,875 | $44,300 |
$39,875
-
kWh
|
- | |
TOTAL RECOMMENDED | $336,170 | $95,548 |
$39,875
-
kWh
|
$296,295
-
MMBtu
|
||
TOTAL IMPLEMENTED | $336,170 | $95,548 |
$39,875
-
kWh
|
$296,295
-
MMBtu
|
||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Coal Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs