| Assessment Year | 2022 |
|---|---|
| Principal Product | Steel Fabrication |
| NAICS | 332322: Sheet Metal Work Manufacturing |
| SIC | 3443: Fabricated Plate Work (Boiler Shops) |
| Sales Range | $10 M to 50M |
| # of Employees | 64 |
| Plant Area |
122,186
ft2
|
| Annual Production | 100,000
units
|
| Production Hrs. Annual | 7,300
hrs
|
| Location (State) | New York |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | |
|---|---|---|---|---|
| Electricity Usage | $59,912 | 1,608,956 |
kWh
|
$0.037 |
| Electricity Demand | $64,451 | 5,647 |
kW-mo/yr
|
$11.41 |
| Electricity Fees | $13,172 | - |
|
- |
| Natural Gas | $55,824 | 11,587 |
MMBtu
|
$4.82 |
| TOTAL YEARLY COSTS | $193,358 | |||
| RECOMMENDED SAVINGS* | $166,537 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
| IMPLEMENTED SAVINGS* | - | |||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | One-time Revenue or Avoided Cost Savings |
|---|---|---|---|---|---|---|---|---|
| 01 | 2.4314: Use synthetic lubricant | $540 | - |
$226
6,092
kWh
|
$315
-
kW-mo/yr
|
- | - | |
| 02 | 2.3131: Reschedule plant operations or reduce load to avoid peaks | $6,448 | $758 | - |
$6,448
-
kW-mo/yr
|
- | - | |
| 03 | 2.1321: Replace fossil fuel equipment with electrical equipment | $147,518 | $63,000 |
$(-7,108.9)
(-191,100)
kWh
|
- | - | $154,627 | |
| 04 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $7,573 | $5,527 |
$4,890
131,450
kWh
|
$2,466
-
kW-mo/yr
|
- | $217 | |
| 05 | 2.7447: Install vinyl strip / high speed / air curtain doors | $3,727 | $4,920 |
$(-68.8)
(-1,850)
kWh
|
- |
$3,796
-
MMBtu
|
- | |
| 06 | 2.7314: Reduce ventilation air | $557 | $882 |
$227
6,114
kWh
|
- |
$329
-
MMBtu
|
- | |
| 07 | 2.4239: Eliminate or reduce compressed air usage | $173 | $831 |
$173
4,677
kWh
|
- | - | - | |
| TOTAL RECOMMENDED | $166,537 | $75,917 |
$(-1,661.8)
(-44,617)
kWh
|
$9,229
-
kW-mo/yr
|
$4,125
-
MMBtu
|
$154,845 | ||
| TOTAL IMPLEMENTED | - | - | - | - | - | - | ||
| Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | One-time Revenue or Avoided Cost Savings | |||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs