| Assessment Year | 2016 |
|---|---|
| Principal Product | Production machine and job shop |
| NAICS | 333517: Machine Tool Manufacturing |
| SIC | 3599: Industrial and Commercial Machinery and Equipment, Not Elsewhere Classified |
| Sales Range | $5 M to 10M |
| # of Employees | 25 |
| Plant Area |
26,548
ft2
|
| Annual Production | 960,000
lb
|
| Production Hrs. Annual | 4,743
hrs
|
| Location (State) | New York |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | ||
|---|---|---|---|---|---|
| Electricity Usage | $26,878 | 392,960 |
kWh
|
$0.068 | |
| Electricity Demand | $18,057 | 1,766 |
kW-mo/yr
|
$10.22 | |
| Electricity Fees | $5,437 | - |
|
- | |
| Natural Gas | $1,664 | 181 |
MMBtu
|
$9.19 | |
| Waste Disposal Costs | |||||
| Water Usage | $826 | 70,000 |
Tgal
|
$0.012 | |
| TOTAL YEARLY COSTS | $52,861 | ||||
| RECOMMENDED SAVINGS* | $4,182 |
See individual recommendations below
*Non-energy impacts included in savings.
|
|||
| IMPLEMENTED SAVINGS* | $4,182 | ||||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Personnel Changes Savings | One-time Revenue or Avoided Cost Savings |
|---|---|---|---|---|---|---|---|---|---|
| 01 | 2.8121: Apply for tax-free status for energy purchases | $1,548 | - | - | - | - | - | $1,548 | |
| 02 | 2.7122: Disconnect ballasts | $145 | - |
$86
1,224
kWh
|
$59
-
kW-mo/yr
|
- | - | - | |
| 03 | 4.821: Pay bills on time to avoid late fees | $30 | - | - | - | - | - | $30 | |
| 04 | 3.1161: Eliminate/reduce an operation | $1,305 | $800 |
$(-43.0)
(-608)
kWh
|
$(-552.0)
-
kW-mo/yr
|
- | $802 | $1,098 | |
| 05 | 2.7314: Reduce ventilation air | $346 | $512 |
$96
1,372
kWh
|
- |
$250
-
MMBtu
|
- | - | |
| 06 | 2.4321: Upgrade obsolete equipment | $42 | $114 |
$35
499
kWh
|
$7
-
kW-mo/yr
|
- | - | - | |
| 07 | 2.4221: Install compressor air intakes in coolest locations | $293 | $778 |
$293
4,180
kWh
|
- | - | - | - | |
| 08 | 3.7312: Implement a regular maintenance program to reduce emissions from leaky valves and pipe fittings | $473 | $1,875 |
$473
6,753
kWh
|
- | - | - | - | |
| TOTAL RECOMMENDED | $4,182 | $4,079 |
$940
13,420
kWh
|
$(-486.0)
-
kW-mo/yr
|
$250
-
MMBtu
|
$802 | $2,676 | ||
| TOTAL IMPLEMENTED | $4,182 | $4,079 |
$940
13,420
kWh
|
$(-486.0)
-
kW-mo/yr
|
$250
-
MMBtu
|
$802 | $2,676 | ||
| Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Personnel Changes Savings | One-time Revenue or Avoided Cost Savings | |||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs