Assessment Year | 1986 |
---|---|
Principal Product | LIQUEFIED GASES |
NAICS |
n/a
|
SIC | 2813: Industrial Gases |
Sales Range | $10 M to 50M |
# of Employees | 45 |
Plant Area |
n/a
|
Annual Production | 164,250
ton
|
Production Hrs. Annual | 8,736
hrs
|
Location (State) | New York |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $4,385,140 | 124,878,665 |
kWh
|
$0.035 |
Fuel Oil #2 | $75,785 | 11,788 |
MMBtu
|
$6.43 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $108,312 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $16,579 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Fuel Oil #2 Savings |
---|---|---|---|---|---|---|
01 | 2.1233: Analyze flue gas for proper air/fuel ratio | $1,364 | $537 | - |
$1,364
-
MMBtu
|
|
02 | 2.7261: Install timers and/or thermostats | $9,159 | $1,000 |
$9,159
260,844
kWh
|
- | |
03 | 2.6121: Reduce hot water temperature to the minimum required | $108 | - |
$108
3,224
kWh
|
- | |
04 | 2.2135: Repair and eliminate steam leaks | $5,948 | $500 | - |
$5,948
-
MMBtu
|
|
05 | 2.4311: Recover mechanical energy | $91,733 | $135,000 |
$91,733
2,613,716
kWh
|
- | |
TOTAL RECOMMENDED | $108,312 | $137,037 |
$101,000
2,877,784
kWh
|
$7,312
-
MMBtu
|
||
TOTAL IMPLEMENTED | $16,579 | $2,037 |
$9,267
264,068
kWh
|
$7,312
-
MMBtu
|
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs