Assessment Year | 2017 |
---|---|
Principal Product | Aluminum Extrusions |
NAICS | 331318: Other Aluminum Rolling, Drawing, and Extruding |
SIC | 3354: Aluminum Extruded Products |
Sales Range | $50 M to 100M |
# of Employees | 110 |
Plant Area |
143,000
ft2
|
Annual Production | 26,000,000
units
|
Production Hrs. Annual | 6,240
hrs
|
Location (State) | Washington |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $336,057 | 6,616,050 |
kWh
|
$0.051 |
Electricity Demand | $91,933 | 15,477 |
kW-mo/yr
|
$5.94 |
Electricity Fees | $28,741 | - |
|
- |
Natural Gas | $93,553 | 17,248 |
MMBtu
|
$5.42 |
TOTAL YEARLY COSTS | $550,284 | |||
RECOMMENDED SAVINGS* | $61,830 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $23,938 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Personnel Changes Savings | Ancillary Material Cost Savings |
---|---|---|---|---|---|---|---|---|---|
01 | 2.1113: Reduce combustion air flow to optimum | $19,831 | $19,940 | - | - |
$19,831
-
MMBtu
|
- | - | |
02 | 2.4224: Upgrade controls on compressors | $16,054 | $2,000 |
$16,054
345,627
kWh
|
- | - | - | - | |
03 | 2.1113: Reduce combustion air flow to optimum | $4,107 | $670 | - | - |
$4,107
-
MMBtu
|
- | - | |
04 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $7,828 | $17,274 |
$7,828
168,527
kWh
|
- | - | - | - | |
05 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $9,688 | $32,940 |
$9,548
205,546
kWh
|
$2,348
-
kW-mo/yr
|
- | $266 | $(-2,474.0) | |
06 | 2.4226: Use / purchase optimum sized compressor | $2,456 | $10,125 |
$2,079
44,768
kWh
|
$376
-
kW-mo/yr
|
- | - | - | |
07 | 2.1113: Reduce combustion air flow to optimum | $1,866 | $5,700 | - | - |
$1,866
-
MMBtu
|
- | - | |
TOTAL RECOMMENDED | $61,830 | $88,649 |
$35,509
764,468
kWh
|
$2,724
-
kW-mo/yr
|
$25,804
-
MMBtu
|
$266 | $(-2,474.0) | ||
TOTAL IMPLEMENTED | $23,938 | $20,610 | - | - |
$23,938
-
MMBtu
|
- | - | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Personnel Changes Savings | Ancillary Material Cost Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs