Assessment Year | 1995 |
---|---|
Principal Product | Steel Parts |
NAICS |
n/a
|
SIC | 3325: Steel Foundries, Not Elsewhere Classified |
Sales Range | $10 M to 50M |
# of Employees | 115 |
Plant Area |
413,800
ft2
|
Annual Production | 11,600,000
lb
|
Production Hrs. Annual | 7,200
hrs
|
Location (State) | Oregon |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $451,313 | 10,461,020 |
kWh
|
$0.043 |
LPG | $139,380 | 24,900 |
MMBtu
|
$5.60 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $34,589 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $20,189 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | LPG Savings |
---|---|---|---|---|---|---|
01 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $17,764 | $14,938 |
$17,764
450,469
kWh
|
- | |
02 | 2.4224: Upgrade controls on compressors | $1,725 | $200 |
$1,725
37,515
kWh
|
- | |
03 | 2.4133: Use most efficient type of electric motors | $700 | $1,195 |
$700
16,706
kWh
|
- | |
04 | 2.2511: Insulate bare equipment | $14,400 | $5,385 | - |
$14,400
-
MMBtu
|
|
TOTAL RECOMMENDED | $34,589 | $21,718 |
$20,189
504,690
kWh
|
$14,400
-
MMBtu
|
||
TOTAL IMPLEMENTED | $20,189 | $16,333 |
$20,189
504,690
kWh
|
- |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs