Assessment Year | 1992 |
---|---|
Principal Product | HEAT EXCHANGERS |
NAICS |
n/a
|
SIC | 3443: Fabricated Plate Work (Boiler Shops) |
Sales Range | $10 M to 50M |
# of Employees | 200 |
Plant Area |
n/a
|
Annual Production | 715
pieces
|
Production Hrs. Annual | 7,488
hrs
|
Location (State) | Oklahoma |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $160,430 | 3,633,353 |
kWh
|
$0.044 |
Natural Gas | $46,201 | 16,761 |
MMBtu
|
$2.76 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $34,198 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $18,321 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|
01 | 2.4221: Install compressor air intakes in coolest locations | $6,587 | $150 |
$6,737
217,468
kWh
|
- | $(-150.0) | |
02 | 2.2511: Insulate bare equipment | $374 | $1,389 | - |
$374
-
MMBtu
|
- | |
03 | 2.2437: Recover waste heat from equipment | $11,360 | $1,185 | - |
$11,360
-
MMBtu
|
- | |
04 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $13,183 | $26,505 |
$13,183
340,563
kWh
|
- | - | |
05 | 2.4231: Reduce the pressure of compressed air to the minimum required | $2,694 | - |
$2,694
69,754
kWh
|
- | - | |
TOTAL RECOMMENDED | $34,198 | $29,229 |
$22,614
627,785
kWh
|
$11,734
-
MMBtu
|
$(-150.0) | ||
TOTAL IMPLEMENTED | $18,321 | $2,724 |
$6,737
217,468
kWh
|
$11,734
-
MMBtu
|
$(-150.0) |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs