Assessment Year | 1987 |
---|---|
Principal Product | REFURBISHED RAIL CARS |
NAICS |
n/a
|
SIC | 3743: Railroad Equipment |
Sales Range | $1 M to 5M |
# of Employees | 44 |
Plant Area |
n/a
|
Annual Production | 1,000
pieces
|
Production Hrs. Annual | 4,160
hrs
|
Location (State) | Oklahoma |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $148,829 | 2,325,909 |
kWh
|
$0.064 |
Natural Gas | $42,314 | 11,067 |
MMBtu
|
$3.82 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $19,231 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $2,397 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|
01 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $2,397 | - |
$2,517
39,273
kWh
|
- | $(-120.0) | |
02 | 2.7261: Install timers and/or thermostats | $16,197 | $1,400 | - |
$16,197
-
MMBtu
|
- | |
03 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $637 | $668 |
$612
9,672
kWh
|
- | $25 | |
TOTAL RECOMMENDED | $19,231 | $2,068 |
$3,129
48,945
kWh
|
$16,197
-
MMBtu
|
$(-95.0) | ||
TOTAL IMPLEMENTED | $2,397 | - |
$2,517
39,273
kWh
|
- | $(-120.0) |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs