Assessment Year | 1985 |
---|---|
Principal Product | COMMERCIAL PRINTING |
NAICS |
n/a
|
SIC | 2761: Manifold Business Forms |
Sales Range | $1 M to 5M |
# of Employees | 45 |
Plant Area |
n/a
|
Annual Production | 0
units
|
Production Hrs. Annual | 0
hrs
|
Location (State) | Oklahoma |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $23,392 | 343,787 |
kWh
|
$0.068 |
Natural Gas | $9,534 | 1,997 |
MMBtu
|
$4.77 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $4,966 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $4,056 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
---|---|---|---|---|---|---|
01 | 2.7224: Reduce space conditioning during non-working hours | $400 | - | - |
$400
-
MMBtu
|
|
02 | 2.7224: Reduce space conditioning during non-working hours | $300 | - | - |
$300
-
MMBtu
|
|
03 | 2.2443: Re-use or recycle hot or cold process exhaust air | $130 | $130 | - |
$130
-
MMBtu
|
|
04 | 2.7221: Lower temperature during the winter season and vice-versa | $1,480 | $975 | - |
$1,480
-
MMBtu
|
|
05 | 2.7121: Utilize daylight whenever possible in lieu of artificial light | $165 | $52 |
$165
2,638
kWh
|
- | |
06 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $1,436 | $885 |
$1,436
19,343
kWh
|
- | |
07 | 2.6232: Install set-back timers | $380 | $90 |
$380
6,448
kWh
|
- | |
08 | 2.2136: Install / repair insulation on steam lines | $675 | $175 | - |
$675
-
MMBtu
|
|
TOTAL RECOMMENDED | $4,966 | $2,307 |
$1,981
28,429
kWh
|
$2,985
-
MMBtu
|
||
TOTAL IMPLEMENTED | $4,056 | $2,087 |
$1,601
21,981
kWh
|
$2,455
-
MMBtu
|
||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs