ITAC Assessment: NC0043
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ITAC Assessment: NC0043
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Assessment Year 1994
Principal Product Ladies Hosiery
NAICS
n/a
SIC 2251: Women's Full-Length and Knee-Length Hosiery, Except Socks
Sales Range $10
M
to 50
M
# of Employees 170
Plant Area 90,000
ft2
Annual Production 0
units
Production Hrs. Annual 4,000
hrs
Location (State) North Carolina

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $115,546 1,858,441
kWh
Natural Gas $114,783 31,451
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $32,070 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $10,423

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Natural Gas Savings
01 2.7142: Utilize higher efficiency lamps and/or ballasts $2,151 $1,502 $2,151
35,756
kWh
-
02 2.7142: Utilize higher efficiency lamps and/or ballasts $8,024 $13,329 $8,024
168,523
kWh
-
03 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves $248 $120 $248
4,103
kWh
-
04 2.4221: Install compressor air intakes in coolest locations $198 $310 $198
3,224
kWh
-
05 2.2437: Recover waste heat from equipment $515 $1,300 - $515
-
MMBtu
06 2.2525: Eliminate cooling of process streams which subsequently must be heated and vice versa $4,592 $27,887 - $4,592
-
MMBtu
07 2.2449: Recover heat from exhausted steam, hot air or hot water $16,342 $10,000 - $16,342
-
MMBtu
TOTAL RECOMMENDED $32,070 $54,448 $10,621
211,606
kWh
$21,449
-
MMBtu
TOTAL IMPLEMENTED $10,423 $14,951 $10,423
208,382
kWh
-
Yearly Savings* Imp'd Cost* Electricity Usage Savings Natural Gas Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs