Assessment Year | 2004 |
---|---|
Principal Product | Wire Cloth |
NAICS | 332618: Other Fabricated Wire Product Manufacturing |
SIC | 3496: Miscellaneous Fabricated Wire Products |
Sales Range | $10 M to 50M |
# of Employees | 100 |
Plant Area |
165,000
ft2
|
Annual Production | 1,000
thousand feet
|
Production Hrs. Annual | 8,400
hrs
|
Location (State) | Mississippi |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $195,007 | 4,376,577 |
kWh
|
$0.045 |
Electricity Demand | $36,203 | 10,295 |
kW-mo/yr
|
$3.52 |
Electricity Fees | $81,873 | - |
|
- |
Natural Gas | $26,476 | 2,818 |
MMBtu
|
$9.40 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $59,385 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $38,455 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Electricity Fees Savings | Natural Gas Savings | Other Liquid (non-haz) Savings |
---|---|---|---|---|---|---|---|---|---|
01 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $36,775 | $59,467 |
$18,681
560,519
kWh
|
$2,804
-
kW-mo/yr
|
$15,290 | - | - | |
02 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $10,523 | $32,157 |
$5,341
160,261
kWh
|
$809
-
kW-mo/yr
|
$4,373 | - | - | |
03 | 2.7124: Make a practice of turning off lights when not needed | $5,480 | $2,430 |
$3,069
92,084
kWh
|
- | $2,411 | - | - | |
04 | 3.6124: Burn waste oil for heat | $3,362 | $3,129 | - | - | - |
$1,362
-
MMBtu
|
$2,000
-
gal
|
|
05 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $1,680 | $189 |
$941
28,245
kWh
|
- | $739 | - | - | |
06 | 2.7261: Install timers and/or thermostats | $791 | $472 |
$443
13,291
kWh
|
- | $348 | - | - | |
07 | 2.6214: Shut off pilots in standby equipment | $774 | $176 | - | - | - |
$774
-
MMBtu
|
- | |
TOTAL RECOMMENDED | $59,385 | $98,020 |
$28,475
854,400
kWh
|
$3,613
-
kW-mo/yr
|
$23,161 |
$2,136
-
MMBtu
|
$2,000
-
gal
|
||
TOTAL IMPLEMENTED | $38,455 | $59,656 |
$19,622
588,764
kWh
|
$2,804
-
kW-mo/yr
|
$16,029 | - | - | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Electricity Fees Savings | Natural Gas Savings | Other Liquid (non-haz) Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs