ITAC Assessment: MO0074
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ITAC Assessment: MO0074
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Assessment Year 1992
Principal Product PLASTIC FOAM PRODUCTS
NAICS
n/a
SIC 3086: Plastics Foam Products
Sales Range $10
M
to 50
M
# of Employees 120
Plant Area
n/a
Annual Production 3,000,000
pieces
Production Hrs. Annual 8,400
hrs
Location (State) Missouri

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $254,687 4,669,109
kWh
Natural Gas $5,859 1,246
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $17,695 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $8,350

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Administrative Changes Savings
01 2.4231: Reduce the pressure of compressed air to the minimum required $4,925 $150 $4,925
90,270
kWh
-
02 2.4221: Install compressor air intakes in coolest locations $4,358 $1,140 $4,358
80,012
kWh
-
03 2.4133: Use most efficient type of electric motors $1,171 $9,000 $1,171
21,395
kWh
-
04 2.4111: Utilize energy-efficient belts and other improved mechanisms $2,254 $280 $2,254
41,325
kWh
-
05 2.7142: Utilize higher efficiency lamps and/or ballasts $2,403 $6,317 $2,403
43,962
kWh
-
06 2.7142: Utilize higher efficiency lamps and/or ballasts $601 $14,500 $657
12,016
kWh
$(-56.0)
07 2.4146: Use adjustable frequency drive or multiple speed motors on existing system $1,983 $329 $1,983
36,342
kWh
-
TOTAL RECOMMENDED $17,695 $31,716 $17,751
325,322
kWh
$(-56.0)
TOTAL IMPLEMENTED $8,350 $9,430 $8,350
152,990
kWh
-
Yearly Savings* Imp'd Cost* Electricity Usage Savings Administrative Changes Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs