Assessment Year | 1995 |
---|---|
Principal Product | Textiles |
NAICS |
n/a
|
SIC | 2542: Office and Store Fixtures, Partitions, Shelving, and Lockers, Except Wood |
Sales Range | $10 M to 50M |
# of Employees | 1,175 |
Plant Area |
423,712
ft2
|
Annual Production | 9,308,000
lb
|
Production Hrs. Annual | 6,000
hrs
|
Location (State) | Maine |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $1,451,047 | 16,418,816 |
kWh
|
$0.088 |
Fuel Oil #2 | $16,443 | 3,877 |
MMBtu
|
$4.24 |
Wood | $238,045 | 160,381 |
MMBtu
|
$1.48 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $118,115 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $3,124 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Wood Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|
01 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $65,514 | $27,280 |
$65,514
358,441
kWh
|
- | - | |
02 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $21,341 | $28,606 |
$21,341
274,619
kWh
|
- | - | |
03 | 2.3511: Use plant owned transformers or lease transformers | $18,499 | $75,000 | - | - | $18,499 | |
04 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $4,642 | $1,200 |
$4,642
66,237
kWh
|
- | - | |
05 | 2.4221: Install compressor air intakes in coolest locations | $3,475 | $1,000 |
$3,475
49,824
kWh
|
- | - | |
06 | 2.1113: Reduce combustion air flow to optimum | $2,205 | $400 | - |
$2,205
-
MMBtu
|
- | |
07 | 2.1311: Replace electrically-operated equipment with fossil fuel equipment | $1,520 | - |
$1,520
24,033
kWh
|
- | - | |
08 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $919 | $1,000 |
$919
13,189
kWh
|
- | - | |
09 | 3.5212: Regrind, reuse, or sell scrap plastic parts | - | - | - | - | - | |
TOTAL RECOMMENDED | $118,115 | $134,486 |
$97,411
786,343
kWh
|
$2,205
-
MMBtu
|
$18,499 | ||
TOTAL IMPLEMENTED | $3,124 | $1,400 |
$919
13,189
kWh
|
$2,205
-
MMBtu
|
- | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Wood Savings | Administrative Changes Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs