Assessment Year | 2001 |
---|---|
Principal Product | Paper |
NAICS |
n/a
|
SIC | 2621: Paper Mills |
Sales Range | $50 M to 100M |
# of Employees | 225 |
Plant Area |
200,000
ft2
|
Annual Production | 40,000
ton
|
Production Hrs. Annual | 8,600
hrs
|
Location (State) | Vermont |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $1,631,300 | 33,006,478 |
kWh
|
$0.049 |
Electricity Demand | $558,531 | 61,285 |
kW-mo/yr
|
$9.11 |
Electricity Fees | $49,571 | - |
|
- |
Fuel Oil #2 | $157,800 | 19,991 |
MMBtu
|
$7.89 |
Fuel Oil #6 | $1,586,800 | 384,636 |
MMBtu
|
$4.13 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $420,825 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $135,125 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Fuel Oil #6 Savings | Ancillary Material Cost Savings | Water Consumption Savings |
---|---|---|---|---|---|---|---|---|---|
01 | 2.2444: Use hot process fluids to preheat incoming process fluids | $241,800 | $250,000 |
$(-25,600.0)
(-513,200)
kWh
|
$(-6,600.0)
-
kW-mo/yr
|
$274,000
-
MMBtu
|
- | - | |
02 | 2.2414: Use waste heat from hot flue gases to preheat | $84,500 | $1,500 | - | - |
$84,500
-
MMBtu
|
- | - | |
03 | 3.4151: Minimize water usage | $25,000 | - | - | - | - | - |
$25,000
-
Tgal
|
|
04 | 3.4141: Replace the chlorination stage with an oxygen or ozone stage | $24,500 | $5,000 | - | - | - | $(-13,500.0) |
$38,000
-
Tgal
|
|
05 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $10,500 | $20,000 |
$10,500
211,000
kWh
|
- | - | - | - | |
06 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $6,025 | $700 |
$6,025
120,500
kWh
|
- | - | - | - | |
07 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $5,800 | - |
$5,800
116,000
kWh
|
- | - | - | - | |
08 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $5,000 | $12,000 |
$5,000
99,000
kWh
|
- | - | - | - | |
09 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $4,900 | $8,000 |
$4,900
97,400
kWh
|
- | - | - | - | |
10 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $3,700 | $7,500 |
$3,700
74,000
kWh
|
- | - | - | - | |
11 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $3,000 | $8,000 |
$3,000
60,500
kWh
|
- | - | - | - | |
12 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $3,000 | $8,000 |
$3,000
62,500
kWh
|
- | - | - | - | |
13 | 2.4221: Install compressor air intakes in coolest locations | $2,900 | $1,000 |
$2,900
57,700
kWh
|
- | - | - | - | |
14 | 2.2136: Install / repair insulation on steam lines | $200 | $150 | - | - |
$200
-
MMBtu
|
- | - | |
TOTAL RECOMMENDED | $420,825 | $321,850 |
$19,225
385,400
kWh
|
$(-6,600.0)
-
kW-mo/yr
|
$358,700
-
MMBtu
|
$(-13,500.0) |
$63,000
-
Tgal
|
||
TOTAL IMPLEMENTED | $135,125 | $29,850 |
$25,425
506,900
kWh
|
- |
$84,700
-
MMBtu
|
- |
$25,000
-
Tgal
|
||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Fuel Oil #6 Savings | Ancillary Material Cost Savings | Water Consumption Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs