Assessment Year | 2020 |
---|---|
Principal Product | Steel Storage Tanks |
NAICS | 332420: Metal Tank (Heavy Gauge) Manufacturing |
SIC | 3443: Fabricated Plate Work (Boiler Shops) |
Sales Range | $10 M to 50M |
# of Employees | 23 |
Plant Area |
120,000
ft2
|
Annual Production | 100
units
|
Production Hrs. Annual | 4,212
hrs
|
Location (State) | Pennsylvania |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $135,855 | 2,084,050 |
kWh
|
$0.065 |
Electricity Demand | $22,380 | 7,967 |
kW-mo/yr
|
$2.81 |
Electricity Fees | $6,917 | - |
|
- |
Natural Gas | $72,503 | 7,252 |
MMBtu
|
$10.00 |
Fuel Oil #1 | $11,310 | 561 |
MMBtu
|
$20.16 |
Fuel Oil #2 | $9,094 | 546 |
MMBtu
|
$16.66 |
TOTAL YEARLY COSTS | $258,059 | |||
RECOMMENDED SAVINGS* | $45,472 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $23,382 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|---|
01 | 2.7263: Lower compressor pressure through a/c system modification | $3,081 | $48 |
$2,744
42,218
kWh
|
$337
-
kW-mo/yr
|
- | - | |
02 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $7,293 | $12,000 |
$5,970
91,841
kWh
|
$1,323
-
kW-mo/yr
|
- | - | |
03 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $5,609 | $10,500 |
$5,106
78,554
kWh
|
$503
-
kW-mo/yr
|
- | - | |
04 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $4,208 | $8,000 |
$3,444
52,986
kWh
|
$764
-
kW-mo/yr
|
- | - | |
05 | 2.2437: Recover waste heat from equipment | $5,400 | $12,000 | - | - |
$5,400
-
MMBtu
|
- | |
06 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $8,668 | $21,820 |
$7,803
120,042
kWh
|
$865
-
kW-mo/yr
|
- | - | |
07 | 2.1332: Convert combustion equipment to burn natural gas | $9,314 | $30,000 | - | - | - | $9,314 | |
08 | 2.7232: Replace existing hvac unit with high efficiency model | $1,899 | $7,200 |
$1,697
26,112
kWh
|
$202
-
kW-mo/yr
|
- | - | |
TOTAL RECOMMENDED | $45,472 | $101,568 |
$26,764
411,753
kWh
|
$3,994
-
kW-mo/yr
|
$5,400
-
MMBtu
|
$9,314 | ||
TOTAL IMPLEMENTED | $23,382 | $63,820 |
$7,803
120,042
kWh
|
$865
-
kW-mo/yr
|
$5,400
-
MMBtu
|
$9,314 | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Administrative Changes Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs