ITAC Assessment: LE0366
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ITAC Assessment: LE0366
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Assessment Year 2013
Principal Product Large Caliber Ammunition Metal Parts
NAICS 332993: Ammunition (except Small Arms) Manufacturing
SIC 3483: Ammunition, Except for Small Arms
Sales Range $50
M
to 100
M
# of Employees 190
Plant Area 500,000
ft2
Annual Production 22,000,000
lb
Production Hrs. Annual 2,080
hrs
Location (State) Pennsylvania

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $2,144,030 30,629,000
kWh
Natural Gas $1,110,999 228,224
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $561,460 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* -

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Natural Gas Savings Ancillary Material Cost Savings
01 2.7142: Utilize higher efficiency lamps and/or ballasts $264,361 $119,173 $262,587
3,751,239
kWh
- $1,774
02 2.2515: Use optimum thickness insulation $45,077 $26,012 - $45,077
-
MMBtu
-
03 2.2511: Insulate bare equipment $2,504 $1,586 - $2,504
-
MMBtu
-
04 3.1161: Eliminate/reduce an operation $13,661 - - - $13,661
05 2.4146: Use adjustable frequency drive or multiple speed motors on existing system $92,173 $61,200 $92,173
1,316,752
kWh
- -
06 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves $3,758 $10,000 $3,758
53,688
kWh
- -
07 2.4146: Use adjustable frequency drive or multiple speed motors on existing system $42,595 $169,520 $42,595
608,502
kWh
- -
08 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves $5,664 $1,000 $5,664
80,917
kWh
- -
09 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves $3,762 $6,498 $3,762
53,753
kWh
- -
10 2.2135: Repair and eliminate steam leaks $51,910 $52,314 - $51,910
-
MMBtu
-
11 2.2136: Install / repair insulation on steam lines $17,390 $6,750 - $17,390
-
MMBtu
-
12 2.2442: Preheat combustion air with waste heat $13,454 $60,000 - $13,454
-
MMBtu
-
13 2.1211: Move boiler to more efficient location $721 $2,000 - $721
-
MMBtu
-
14 2.4322: Use or replace with energy efficient substitutes $3,188 $11,909 $3,188
45,552
kWh
- -
15 2.7261: Install timers and/or thermostats $1,242 $2,400 $1,242
17,736
kWh
- -
TOTAL RECOMMENDED $561,460 $530,362 $414,969
5,928,139
kWh
$131,056
-
MMBtu
$15,435
TOTAL IMPLEMENTED - - - - -
Yearly Savings* Imp'd Cost* Electricity Usage Savings Natural Gas Savings Ancillary Material Cost Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs