Assessment Year | 1987 |
---|---|
Principal Product | LAB APPARATUS |
NAICS |
n/a
|
SIC | 3821: Laboratory Apparatus and Furniture |
Sales Range | $10 M to 50M |
# of Employees | 200 |
Plant Area |
n/a
|
Annual Production | 1,000
pieces
|
Production Hrs. Annual | 4,160
hrs
|
Location (State) | Missouri |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $138,387 | 1,676,729 |
kWh
|
$0.083 |
Natural Gas | $49,291 | 13,023 |
MMBtu
|
$3.78 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $16,908 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $7,733 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|
01 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $4,144 | $615 |
$4,144
49,531
kWh
|
- | - | |
02 | 2.3191: Use demand controller or load shedder | $3,808 | $1,200 |
$3,808
-
kWh
|
- | - | |
03 | 2.2447: Heat water with exhaust heat | $3,795 | $7,000 | - |
$3,795
-
MMBtu
|
- | |
04 | 2.1123: Install automatic stack damper | $1,486 | $2,600 | - |
$1,486
-
MMBtu
|
- | |
05 | 2.1233: Analyze flue gas for proper air/fuel ratio | $1,040 | - | - |
$1,300
-
MMBtu
|
$(-260.0) | |
06 | 2.4312: Improve lubrication practices | $677 | $400 |
$677
8,206
kWh
|
- | - | |
07 | 2.4231: Reduce the pressure of compressed air to the minimum required | $605 | $90 |
$605
7,327
kWh
|
- | - | |
08 | 2.6214: Shut off pilots in standby equipment | $437 | - | - |
$537
-
MMBtu
|
$(-100.0) | |
09 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $314 | $205 |
$314
3,810
kWh
|
- | - | |
10 | 2.4221: Install compressor air intakes in coolest locations | $290 | $500 |
$290
3,517
kWh
|
- | - | |
11 | 2.6121: Reduce hot water temperature to the minimum required | $191 | - | - |
$191
-
MMBtu
|
- | |
12 | 2.4111: Utilize energy-efficient belts and other improved mechanisms | $121 | $520 |
$121
1,465
kWh
|
- | - | |
TOTAL RECOMMENDED | $16,908 | $13,130 |
$9,959
73,856
kWh
|
$7,309
-
MMBtu
|
$(-360.0) | ||
TOTAL IMPLEMENTED | $7,733 | $3,940 |
$4,579
54,806
kWh
|
$3,514
-
MMBtu
|
$(-360.0) | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs