Assessment Year | 2016 |
---|---|
Principal Product | Automotive Parts |
NAICS | 336350: Motor Vehicle Transmission and Power Train Parts Manufacturing |
SIC | 3714: Motor Vehicle Parts and Accessories |
Sales Range | $100 M to 500M |
# of Employees | 300 |
Plant Area |
211,273
ft2
|
Annual Production | 5,273,031
units
|
Production Hrs. Annual | 8,400
hrs
|
Location (State) | Indiana |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $1,304,796 | 22,845,960 |
kWh
|
$0.057 |
Electricity Demand | $326,704 | 40,274 |
kW-mo/yr
|
$8.11 |
Electricity Fees | $3,148 | - |
|
- |
Natural Gas | $78,600 | 10,641 |
MMBtu
|
$7.39 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $342,664 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $110,930 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Water Disposal Savings | One-time Revenue or Avoided Cost Savings |
---|---|---|---|---|---|---|---|---|---|
01 | 2.4231: Reduce the pressure of compressed air to the minimum required | $7,775 | $4 |
$7,057
123,803
kWh
|
$718
-
kW-mo/yr
|
- | - | - | |
02 | 2.4323: Use optimum size and capacity equipment | $2,745 | - |
$2,297
40,296
kWh
|
$448
-
kW-mo/yr
|
- | - | - | |
03 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $2,196 | $35 |
$2,196
38,528
kWh
|
- | - | - | - | |
04 | 2.7224: Reduce space conditioning during non-working hours | $931 | $20 | - | - |
$931
-
MMBtu
|
- | - | |
05 | 2.7135: Install occupancy sensors | $5,310 | $1,611 |
$5,310
93,154
kWh
|
- | - | - | - | |
06 | 2.7232: Replace existing hvac unit with high efficiency model | $9,664 | $3,260 |
$5,054
88,667
kWh
|
$4,610
-
kW-mo/yr
|
- | - | - | |
07 | 2.4322: Use or replace with energy efficient substitutes | $1,734 | $760 |
$1,734
30,416
kWh
|
- | - | - | - | |
08 | 3.5131: Recycle white water | $61,804 | $36,000 | - | - | - |
$61,804
-
Tgal
|
- | |
09 | 4.631: Install an uninteruptable power supply | $230,000 | $251,000 | - | - | - | - | $230,000 | |
10 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $20,505 | $75,569 |
$16,711
293,173
kWh
|
$3,794
-
kW-mo/yr
|
- | - | - | |
TOTAL RECOMMENDED | $342,664 | $368,259 |
$40,359
708,037
kWh
|
$9,570
-
kW-mo/yr
|
$931
-
MMBtu
|
$61,804
-
Tgal
|
$230,000 | ||
TOTAL IMPLEMENTED | $110,930 | $116,499 |
$38,625
677,621
kWh
|
$9,570
-
kW-mo/yr
|
$931
-
MMBtu
|
$61,804
-
Tgal
|
- | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Water Disposal Savings | One-time Revenue or Avoided Cost Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs