ITAC Assessment: HO0103
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ITAC Assessment: HO0103
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Assessment Year 1995
Principal Product Metal and Plastic Toilet Partitions
NAICS
n/a
SIC 2542: Office and Store Fixtures, Partitions, Shelving, and Lockers, Except Wood
Sales Range $10
M
to 50
M
# of Employees 135
Plant Area 85,000
ft2
Annual Production 57,200
pieces
Production Hrs. Annual 3,595
hrs
Location (State) New York

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $129,826 823,271
kWh
Natural Gas $98,684 12,423
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $62,936 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* -

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Natural Gas Savings Administrative Changes Savings
01 2.7142: Utilize higher efficiency lamps and/or ballasts $5,438 $3,595 n/a $5,438
34,584
kWh
- -
02 2.7142: Utilize higher efficiency lamps and/or ballasts $1,411 $1,970 n/a $1,411
9,086
kWh
- -
03 2.4133: Use most efficient type of electric motors $839 $850 n/a $839
5,275
kWh
- -
04 2.4221: Install compressor air intakes in coolest locations $1,496 $300 n/a $1,496
9,672
kWh
- -
05 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves $5,217 $250 n/a $5,217
33,118
kWh
- -
06 2.2136: Install / repair insulation on steam lines $654 $1,288 n/a - $654
-
MMBtu
-
07 2.4111: Utilize energy-efficient belts and other improved mechanisms $1,351 $1,060 n/a $1,351
8,499
kWh
- -
08 2.1232: Keep boiler tubes clean $1,303 $1,800 n/a - $1,303
-
MMBtu
-
09 2.8114: Change rate schedules or other changes in utility service $45,227 $50,000 n/a - - $45,227
TOTAL RECOMMENDED $62,936 $61,113 $15,752
100,234
kWh
$1,957
-
MMBtu
$45,227
TOTAL IMPLEMENTED - - - - -
Yearly Savings* Imp'd Cost* Electricity Usage Savings Natural Gas Savings Administrative Changes Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs