ITAC Assessment: AS0019
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ITAC Assessment: AS0019
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Assessment Year 1991
Principal Product OAK BEDROOM FURNITURE
NAICS
n/a
SIC 2511: Wood Household Furniture, Except Upholstered
Sales Range $10
M
to 50
M
# of Employees 75
Plant Area
n/a
Annual Production 0
units
Production Hrs. Annual 2,100
hrs
Location (State) Arizona

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $104,307 1,233,001
kWh
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $14,664 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $14,664

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Natural Gas Savings Administrative Changes Savings
01 2.1311: Replace electrically-operated equipment with fossil fuel equipment $11,610 - $36,449
430,832
kWh
$(-22,089.0)
-
MMBtu
$(-2,750.0)
02 2.7142: Utilize higher efficiency lamps and/or ballasts $95 $155 $95
1,172
kWh
- -
03 2.6232: Install set-back timers $140 $150 $140
1,758
kWh
- -
04 2.6212: Turn off equipment during breaks, reduce operating time $402 $200 $402
4,689
kWh
- -
05 2.4133: Use most efficient type of electric motors $390 $1,560 $390
4,689
kWh
- -
06 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves $696 $500 $696
8,206
kWh
- -
07 2.4231: Reduce the pressure of compressed air to the minimum required $1,331 $1,100 $1,331
15,826
kWh
- -
TOTAL RECOMMENDED $14,664 $3,665 $39,503
467,172
kWh
$(-22,089.0)
-
MMBtu
$(-2,750.0)
TOTAL IMPLEMENTED $14,664 $3,665 $39,503
467,172
kWh
$(-22,089.0)
-
MMBtu
$(-2,750.0)
Yearly Savings* Imp'd Cost* Electricity Usage Savings Natural Gas Savings Administrative Changes Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs