| Assessment Year | 1993 |
|---|---|
| Principal Product | Graphite Electrodes |
| NAICS |
n/a
|
| SIC | 3624: Carbon and Graphite Products |
| Sales Range | $5 M to 10M |
| # of Employees | 94 |
| Plant Area |
108,717
ft2
|
| Annual Production | 4,500
ton
|
| Production Hrs. Annual | 2,080
hrs
|
| Location (State) | Arkansas |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | |
|---|---|---|---|---|
| Electricity Usage | $1,055,064 | 20,121,044 |
kWh
|
$0.052 |
| Natural Gas | $461,974 | 187,519 |
MMBtu
|
$2.46 |
| TOTAL YEARLY COSTS | - | |||
| RECOMMENDED SAVINGS* | $13,837 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
| IMPLEMENTED SAVINGS* | $12,098 | |||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
|---|---|---|---|---|---|---|
| 01 | 2.4221: Install compressor air intakes in coolest locations | $2,244 | $230 |
$2,244
42,790
kWh
|
- | |
| 02 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $7,622 | $620 |
$7,622
145,369
kWh
|
- | |
| 03 | 2.4131: Size electric motors for peak operating efficiency | $1,739 | $600 |
$1,739
33,118
kWh
|
- | |
| 04 | 2.2135: Repair and eliminate steam leaks | $1,845 | $475 | - |
$1,845
-
MMBtu
|
|
| 05 | 2.1233: Analyze flue gas for proper air/fuel ratio | $387 | $1,000 | - |
$387
-
MMBtu
|
|
| TOTAL RECOMMENDED | $13,837 | $2,925 |
$11,605
221,277
kWh
|
$2,232
-
MMBtu
|
||
| TOTAL IMPLEMENTED | $12,098 | $2,325 |
$9,866
188,159
kWh
|
$2,232
-
MMBtu
|
||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs