Assessment Year | 1995 |
---|---|
Principal Product | application tapes |
NAICS |
n/a
|
SIC | 2672: Coated and Laminated Paper, Not Elsewhere Classified |
Sales Range | $10 M to 50M |
# of Employees | 125 |
Plant Area |
60,000
ft2
|
Annual Production | 216,000
pieces
|
Production Hrs. Annual | 6,000
hrs
|
Location (State) | Wisconsin |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $154,940 | 3,098,769 |
kWh
|
$0.050 |
Natural Gas | $144,866 | 41,622 |
MMBtu
|
$3.48 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $22,397 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $8,339 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|
01 | 2.8121: Apply for tax-free status for energy purchases | $12,947 | - | - | - | $12,947 | |
02 | 2.7221: Lower temperature during the winter season and vice-versa | $3,633 | - | - |
$3,633
-
MMBtu
|
- | |
03 | 2.2511: Insulate bare equipment | $2,042 | $2,089 | - |
$2,042
-
MMBtu
|
- | |
04 | 2.2511: Insulate bare equipment | $442 | $585 | - |
$442
-
MMBtu
|
- | |
05 | 2.1233: Analyze flue gas for proper air/fuel ratio | $1,124 | $500 | - |
$1,124
-
MMBtu
|
- | |
06 | 2.3131: Reschedule plant operations or reduce load to avoid peaks | $1,111 | - |
$1,111
-
kWh
|
- | - | |
07 | 2.3132: Recharge batteries on during off-peak demand periods | $1,098 | - |
$1,098
-
kWh
|
- | - | |
TOTAL RECOMMENDED | $22,397 | $3,174 |
$2,209
-
kWh
|
$7,241
-
MMBtu
|
$12,947 | ||
TOTAL IMPLEMENTED | $8,339 | $3,174 |
$1,098
-
kWh
|
$7,241
-
MMBtu
|
- | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs