ITAC Assessment: UF0317
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ITAC Assessment: UF0317
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Assessment Year 2003
Principal Product Corrugated Cardboard Boxes
NAICS 322211: Corrugated and Solid Fiber Box Manufacturing
SIC 2653: Corrugated and Solid Fiber Boxes
Sales Range $10
M
to 50
M
# of Employees 120
Plant Area 100,000
ft2
Annual Production 100,000,000
pieces
Production Hrs. Annual 7,488
hrs
Location (State) Florida

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $19,985 689,131
kWh
Electricity Demand $4,227 95
kW-mo/yr
Natural Gas $25,640 4,722
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $110,538 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* -

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Electricity Demand Savings Natural Gas Savings Administrative Changes Savings
01 2.7142: Utilize higher efficiency lamps and/or ballasts $12,161 $11,978 n/a $10,247
353,328
kWh
$1,914
-
kW-mo/yr
- -
02 2.7132: Install timers on light switches in little used areas $4,254 $1,640 n/a $4,254
114,985
kWh
- - -
03 2.4133: Use most efficient type of electric motors $6,925 $5,839 n/a $4,914
169,451
kWh
$2,011
-
kW-mo/yr
- -
04 2.3212: Optimize plant power factor $5,621 $15,000 n/a - - - $5,621
05 2.7142: Utilize higher efficiency lamps and/or ballasts $1,795 $7,524 n/a $1,490
51,367
kWh
$305
-
kW-mo/yr
- -
06 2.2135: Repair and eliminate steam leaks $25,640 $120 n/a - - $25,640
-
MMBtu
-
07 4.111: Add equipment/ operators to reduce production bottleneck $6,065 $10,440 n/a - - - $6,065
08 4.322: Eliminate old stock and modify inventory control $48,077 $145,000 n/a - - - $48,077
TOTAL RECOMMENDED $110,538 $197,541 $20,905
689,131
kWh
$4,230
-
kW-mo/yr
$25,640
-
MMBtu
$59,763
TOTAL IMPLEMENTED - - - - - -
Yearly Savings* Imp'd Cost* Electricity Usage Savings Electricity Demand Savings Natural Gas Savings Administrative Changes Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs