Assessment Year | 2008 |
---|---|
Principal Product | Electric Motors |
NAICS | 335312: Motor and Generator Manufacturing |
SIC | 3612: Power, Distribution, and Specialty Transformers |
Sales Range | $10 M to 50M |
# of Employees | 425 |
Plant Area |
59,900
ft2
|
Annual Production | 2,160,000
pieces
|
Production Hrs. Annual | 6,240
hrs
|
Location (State) | Tennessee |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $238,232 | 3,067,800 |
kWh
|
$0.078 |
Natural Gas | $101,666 | 9,380 |
MMBtu
|
$10.84 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $46,334 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $3,637 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|
01 | 2.8114: Change rate schedules or other changes in utility service | $1,297 | $250 | - | - | $1,297 | |
02 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $1,204 | $862 |
$1,204
13,965
kWh
|
- | - | |
03 | 2.4133: Use most efficient type of electric motors | $2,340 | $5,000 |
$2,340
26,004
kWh
|
- | - | |
04 | 2.7121: Utilize daylight whenever possible in lieu of artificial light | $25,272 | $22,000 |
$25,272
280,800
kWh
|
- | - | |
05 | 2.1113: Reduce combustion air flow to optimum | $16,221 | $30,000 | - |
$16,221
-
MMBtu
|
- | |
TOTAL RECOMMENDED | $46,334 | $58,112 |
$28,816
320,769
kWh
|
$16,221
-
MMBtu
|
$1,297 | ||
TOTAL IMPLEMENTED | $3,637 | $5,250 |
$2,340
26,004
kWh
|
- | $1,297 |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs