Assessment Year | 2013 |
---|---|
Principal Product | Oral solid dose pharmaceuticals |
NAICS | 325412: Pharmaceutical Preparation Manufacturing |
SIC | 2834: Pharmaceutical Preparations |
Sales Range | $50 M to 100M |
# of Employees | 414 |
Plant Area |
384,000
ft2
|
Annual Production | 755,000,000
pieces
|
Production Hrs. Annual | 8,760
hrs
|
Location (State) | New York |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $852,904 | 13,822,252 |
kWh
|
$0.062 |
Electricity Demand | $94,722 | 24,343 |
kW-mo/yr
|
$3.89 |
Electricity Fees | $8,522 | - |
|
- |
Natural Gas | $311,556 | 52,292 |
MMBtu
|
$5.96 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $256,101 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $42,923 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Personnel Changes Savings | One-time Revenue or Avoided Cost Savings |
---|---|---|---|---|---|---|---|---|---|
01 | 4.821: Pay bills on time to avoid late fees | $3,233 | - | - | - | - | - | $3,233 | |
02 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $111,890 | $4,878 |
$112,147
1,817,622
kWh
|
$(-257.0)
-
kW-mo/yr
|
- | - | - | |
03 | 4.426: Modify workload | $80,009 | $2,213 | - | - | - | $80,009 | - | |
04 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $39,567 | $2,727 |
$39,567
641,288
kWh
|
- | - | - | - | |
05 | 3.1161: Eliminate/reduce an operation | $11,039 | $5,760 |
$(-107.0)
(-1,733)
kWh
|
$(-280.0)
-
kW-mo/yr
|
- | $1,252 | $10,174 | |
06 | 2.2136: Install / repair insulation on steam lines | $513 | $294 | - | - |
$513
-
MMBtu
|
- | - | |
07 | 2.7444: Close holes and openings in building such as broken windows | $59 | $46 | - | - |
$59
-
MMBtu
|
- | - | |
08 | 2.7314: Reduce ventilation air | $3,034 | $5,294 |
$227
3,682
kWh
|
$28
-
kW-mo/yr
|
$2,779
-
MMBtu
|
- | - | |
09 | 2.2414: Use waste heat from hot flue gases to preheat | $6,693 | $15,784 | - | - |
$6,693
-
MMBtu
|
- | - | |
10 | 2.4321: Upgrade obsolete equipment | $64 | $224 |
$59
964
kWh
|
$5
-
kW-mo/yr
|
- | - | - | |
TOTAL RECOMMENDED | $256,101 | $37,220 |
$151,893
2,461,823
kWh
|
$(-504.0)
-
kW-mo/yr
|
$10,044
-
MMBtu
|
$81,261 | $13,407 | ||
TOTAL IMPLEMENTED | $42,923 | $2,997 |
$39,626
642,252
kWh
|
$5
-
kW-mo/yr
|
$59
-
MMBtu
|
- | $3,233 | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Personnel Changes Savings | One-time Revenue or Avoided Cost Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs