Assessment Year | 2001 |
---|---|
Principal Product | Lumber |
NAICS |
n/a
|
SIC | 2421: Sawmills and Planing Mills, General |
Sales Range | $1 M to 5M |
# of Employees | 18 |
Plant Area |
n/a
|
Annual Production | 42,496
thousand feet
|
Production Hrs. Annual | 4,160
hrs
|
Location (State) | Idaho |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $84,371 | 2,518,560 |
kWh
|
$0.033 |
Electricity Demand | $79,400 | 13,980 |
kW-mo/yr
|
$5.68 |
Electricity Fees | $8,440 | - |
|
- |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $233,471 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $16,128 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Electricity Fees Savings | Ancillary Material Cost Savings | Primary Product Savings |
---|---|---|---|---|---|---|---|---|---|
01 | 4.132: Purchase new equipment to reduce material use / cost | $210,300 | $750,000 | - | - | - | $(-10,000.0) | $220,300 | |
02 | 2.4133: Use most efficient type of electric motors | $7,142 | $20,166 |
$2,644
78,916
kWh
|
$4,498
-
kW-mo/yr
|
- | - | - | |
03 | 2.3212: Optimize plant power factor | $5,776 | $5,800 | - | - | $5,776 | - | - | |
04 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $3,210 | $3,200 |
$1,770
52,970
kWh
|
$1,440
-
kW-mo/yr
|
- | - | - | |
05 | 2.4224: Upgrade controls on compressors | $7,043 | $20,800 |
$3,743
111,728
kWh
|
$3,300
-
kW-mo/yr
|
- | - | - | |
TOTAL RECOMMENDED | $233,471 | $799,966 |
$8,157
243,614
kWh
|
$9,238
-
kW-mo/yr
|
$5,776 | $(-10,000.0) | $220,300 | ||
TOTAL IMPLEMENTED | $16,128 | $29,166 |
$4,414
131,886
kWh
|
$5,938
-
kW-mo/yr
|
$5,776 | - | - |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs