Assessment Year | 1996 |
---|---|
Principal Product | Treated Railroad Ties |
NAICS |
n/a
|
SIC | 2491: Wood Preserving |
Sales Range | $10 M to 50M |
# of Employees | 55 |
Plant Area |
3,500,000
ft2
|
Annual Production | 3,505,832
thousand feet
|
Production Hrs. Annual | 8,760
hrs
|
Location (State) | Oregon |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $62,509 | 2,179,953 |
kWh
|
$0.029 |
Electricity Demand | $16,613 | 8,868 |
kW-mo/yr
|
$1.87 |
Natural Gas | $118,144 | 48,915 |
MMBtu
|
$2.42 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $17,426 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $7,532 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Solid Waste (non-haz) Savings | Personnel Changes Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|---|---|---|
01 | 3.1192: Reduce scrap production | $3,761 | - | - | - | - |
$12,017
-
lb
|
$(-7,680.0) | $(-576.0) | |
02 | 2.1233: Analyze flue gas for proper air/fuel ratio | $9,894 | $500 | - | - |
$9,894
-
MMBtu
|
- | - | - | |
03 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $3,493 | $5,000 |
$2,610
128,664
kWh
|
$883
-
kW-mo/yr
|
- | - | - | - | |
04 | 2.4133: Use most efficient type of electric motors | $278 | $1,091 |
$188
9,379
kWh
|
$90
-
kW-mo/yr
|
- | - | - | - | |
TOTAL RECOMMENDED | $17,426 | $6,591 |
$2,798
138,043
kWh
|
$973
-
kW-mo/yr
|
$9,894
-
MMBtu
|
$12,017
-
lb
|
$(-7,680.0) | $(-576.0) | ||
TOTAL IMPLEMENTED | $7,532 | $6,091 |
$2,798
138,043
kWh
|
$973
-
kW-mo/yr
|
- |
$12,017
-
lb
|
$(-7,680.0) | $(-576.0) |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs