Assessment Year | 1989 |
---|---|
Principal Product | ROCK CRUSHING EQUIPMENT |
NAICS |
n/a
|
SIC | 3531: Construction Machinery and Equipment |
Sales Range | $10 M to 50M |
# of Employees | 210 |
Plant Area |
n/a
|
Annual Production | 276
pieces
|
Production Hrs. Annual | 4,556
hrs
|
Location (State) | Oregon |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $126,105 | 2,395,369 |
kWh
|
$0.053 |
Natural Gas | $38,172 | 7,033 |
MMBtu
|
$5.43 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $16,285 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $8,501 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|
01 | 2.2437: Recover waste heat from equipment | $5,924 | $2,050 | - |
$5,924
-
MMBtu
|
- | |
02 | 2.7111: Reduce illumination to minimum necessary levels | $2,603 | $1,075 |
$2,106
50,703
kWh
|
- | $497 | |
03 | 2.6222: Use drying oven (batch type) on alternate days or other optimum schedule to run equipment with full loads | $338 | $150 |
$338
6,448
kWh
|
- | - | |
04 | 2.4133: Use most efficient type of electric motors | $394 | $279 |
$394
7,327
kWh
|
- | - | |
05 | 2.3212: Optimize plant power factor | $5,181 | $5,400 |
$5,181
-
kWh
|
- | - | |
06 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $1,845 | $2,000 |
$1,845
34,877
kWh
|
- | - | |
TOTAL RECOMMENDED | $16,285 | $10,954 |
$9,864
99,355
kWh
|
$5,924
-
MMBtu
|
$497 | ||
TOTAL IMPLEMENTED | $8,501 | $4,479 |
$2,577
48,652
kWh
|
$5,924
-
MMBtu
|
- | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs