Assessment Year | 2024 |
---|---|
Principal Product | Rebuilt jet engines |
NAICS | 336413: Other Aircraft Parts and Auxiliary Equipment Manufacturing |
SIC | 3728: Aircraft Parts and Auxiliary Equipment, Not Elsewhere Classified |
Sales Range | $1 M to 5M |
# of Employees | 160 |
Plant Area |
271,962
ft2
|
Annual Production | 100
units
|
Production Hrs. Annual | 5,824
hrs
|
Location (State) | Oklahoma |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | ||
---|---|---|---|---|---|
Electricity Usage | $218,807 | 2,485,837 |
kWh
|
$0.088 | |
Electricity Demand | $72,936 | 9,368 |
kW-mo/yr
|
$7.79 | |
Natural Gas | $35,113 | 7,013 |
MMBtu
|
$5.01 | |
Waste Disposal Costs | |||||
Water Usage | $2,233 | 822 |
Tgal
|
$2.72 | |
Water Disposal | $5,713 | 822 |
Tgal
|
$6.95 | |
TOTAL YEARLY COSTS | $334,802 | ||||
RECOMMENDED SAVINGS* | $117,633 |
See individual recommendations below
*Non-energy impacts included in savings.
|
|||
IMPLEMENTED SAVINGS* | $24,474 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings |
---|---|---|---|---|---|---|---|
01 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $12,576 | $44,000 |
$10,021
113,869
kWh
|
$2,555
-
kW-mo/yr
|
- | |
02 | 2.9114: Use solar heat to make electricty | $58,213 | $394,200 |
$58,213
661,510
kWh
|
- | - | |
03 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $8,162 | $3,598 |
$8,162
92,750
kWh
|
- | - | |
04 | 2.6211: Conserve energy by efficient use of vending machines | $213 | $820 |
$213
2,418
kWh
|
- | - | |
05 | 2.7211: Clean and maintain refrigerant condensers and towers | $5,582 | $11,028 |
$5,582
63,434
kWh
|
- | - | |
06 | 2.7232: Replace existing hvac unit with high efficiency model | $5,867 | $38,775 |
$5,867
66,674
kWh
|
- | - | |
07 | 2.3191: Use demand controller or load shedder | $8,413 | $3,850 | - |
$8,413
-
kW-mo/yr
|
- | |
08 | 2.7226: Use computer programs to optimize hvac performance | $18,482 | $120,578 |
$13,562
154,115
kWh
|
- |
$4,920
-
MMBtu
|
|
09 | 2.2622: Replace existing chiller with high efficiency model | $125 | $825 |
$125
1,419
kWh
|
- | - | |
TOTAL RECOMMENDED | $117,633 | $617,674 |
$101,745
1,156,189
kWh
|
$10,968
-
kW-mo/yr
|
$4,920
-
MMBtu
|
||
TOTAL IMPLEMENTED | $24,474 | $160,178 |
$19,554
222,208
kWh
|
- |
$4,920
-
MMBtu
|
||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs