ITAC Assessment: OK0554
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ITAC Assessment: OK0554
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Assessment Year 1998
Principal Product Fans
NAICS
n/a
SIC 3564: Industrial and Commercial Fans and Blowers and Air Purification Equipment
Sales Range $10
M
to 50
M
# of Employees 350
Plant Area 354,418
ft2
Annual Production 85,000
lb
Production Hrs. Annual 4,680
hrs
Location (State) Oklahoma

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $99,919 3,611,958
kWh
Electricity Demand $90,832 -
Natural Gas $122,837 29,175
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $250,659 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $6,636

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Electricity Demand Savings Natural Gas Savings Water Disposal Savings Solid Waste (non-haz) Savings Personnel Changes Savings Ancillary Material Cost Savings
01 2.7142: Utilize higher efficiency lamps and/or ballasts $3,306 $13,340 $2,675
94,373
kWh
$2,174
-
kW-mo/yr
- - - - $(-1,543.0)
02 2.7142: Utilize higher efficiency lamps and/or ballasts $571 $2,830 $373
12,309
kWh
$229
-
kW-mo/yr
- - - - $(-31.0)
03 2.7135: Install occupancy sensors $12,689 $4,620 $12,689
77,374
kWh
- - - - - -
04 2.7142: Utilize higher efficiency lamps and/or ballasts $258 $544 $58
2,052
kWh
$36
-
kW-mo/yr
- - - - $164
05 2.7232: Replace existing hvac unit with high efficiency model $17,170 $97,980 - - $17,170
-
MMBtu
- - - -
06 3.5313: Increase amount of waste recovered for resale $812 - - - - $812
-
Tgal
- - -
07 3.5313: Increase amount of waste recovered for resale $3,600 - - - - - $3,600
-
lb
- -
08 4.514: Re-arrange equipment layout to reduce handling costs $210,600 $120,000 - - - - - $210,600 -
09 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves $1,653 $3,170 $1,653
56,272
kWh
- - - - - -
TOTAL RECOMMENDED $250,659 $242,484 $17,448
242,380
kWh
$2,439
-
kW-mo/yr
$17,170
-
MMBtu
$812
-
Tgal
$3,600
-
lb
$210,600 $(-1,410.0)
TOTAL IMPLEMENTED $6,636 $6,000 $2,026
68,581
kWh
$229
-
kW-mo/yr
- $812
-
Tgal
$3,600
-
lb
- $(-31.0)
Yearly Savings* Imp'd Cost* Electricity Usage Savings Electricity Demand Savings Natural Gas Savings Water Disposal Savings Solid Waste (non-haz) Savings Personnel Changes Savings Ancillary Material Cost Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs