Assessment Year | 1998 |
---|---|
Principal Product | Fans |
NAICS |
n/a
|
SIC | 3564: Industrial and Commercial Fans and Blowers and Air Purification Equipment |
Sales Range | $10 M to 50M |
# of Employees | 350 |
Plant Area |
354,418
ft2
|
Annual Production | 85,000
lb
|
Production Hrs. Annual | 4,680
hrs
|
Location (State) | Oklahoma |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $99,919 | 3,611,958 |
kWh
|
$0.028 |
Electricity Demand | $90,832 | - |
|
- |
Natural Gas | $122,837 | 29,175 |
MMBtu
|
$4.21 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $250,659 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $6,636 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Water Disposal Savings | Solid Waste (non-haz) Savings | Personnel Changes Savings | Ancillary Material Cost Savings |
---|---|---|---|---|---|---|---|---|---|---|---|
01 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $3,306 | $13,340 |
$2,675
94,373
kWh
|
$2,174
-
kW-mo/yr
|
- | - | - | - | $(-1,543.0) | |
02 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $571 | $2,830 |
$373
12,309
kWh
|
$229
-
kW-mo/yr
|
- | - | - | - | $(-31.0) | |
03 | 2.7135: Install occupancy sensors | $12,689 | $4,620 |
$12,689
77,374
kWh
|
- | - | - | - | - | - | |
04 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $258 | $544 |
$58
2,052
kWh
|
$36
-
kW-mo/yr
|
- | - | - | - | $164 | |
05 | 2.7232: Replace existing hvac unit with high efficiency model | $17,170 | $97,980 | - | - |
$17,170
-
MMBtu
|
- | - | - | - | |
06 | 3.5313: Increase amount of waste recovered for resale | $812 | - | - | - | - |
$812
-
Tgal
|
- | - | - | |
07 | 3.5313: Increase amount of waste recovered for resale | $3,600 | - | - | - | - | - |
$3,600
-
lb
|
- | - | |
08 | 4.514: Re-arrange equipment layout to reduce handling costs | $210,600 | $120,000 | - | - | - | - | - | $210,600 | - | |
09 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $1,653 | $3,170 |
$1,653
56,272
kWh
|
- | - | - | - | - | - | |
TOTAL RECOMMENDED | $250,659 | $242,484 |
$17,448
242,380
kWh
|
$2,439
-
kW-mo/yr
|
$17,170
-
MMBtu
|
$812
-
Tgal
|
$3,600
-
lb
|
$210,600 | $(-1,410.0) | ||
TOTAL IMPLEMENTED | $6,636 | $6,000 |
$2,026
68,581
kWh
|
$229
-
kW-mo/yr
|
- |
$812
-
Tgal
|
$3,600
-
lb
|
- | $(-31.0) | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Water Disposal Savings | Solid Waste (non-haz) Savings | Personnel Changes Savings | Ancillary Material Cost Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs